• Title/Summary/Keyword: Multi-rotor

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A Study on the Development of Automatic Measuring System on the Alignment Offset of the Vertical Multistage Shaft (수직형 다단축의 축 정열 오프셋 자동 측정시스템 개발)

  • Park, H.C.;Kim, M.Y.;Lee, H.
    • Journal of KSNVE
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    • v.8 no.5
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    • pp.922-928
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    • 1998
  • This paper presents the automatic alignment measuring system for improving the accuracy and working time of alignment of large vertical hydraulic pump turbine. It is general practice that rotating shaft should run within acceptable vibration limit. In order to obtain better run-out data of multi-stage rotor, careful and accurate alignment approach must be established. Generally, present alignment procedure are required several iterative works and so many manpower. Therefore, the new system has been developed using a vector calculation algorithm, laser sensor and data acquisition devices. As a result of appling to actual machines, it is confirmed that manpower is saved up to an average 90%.

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Conceptual Design and Development Test of an Unmanned Scaled-down Quad Tilt Prop PAV (쿼드 틸트 프롭형 PAV 무인 축소모델 개념설계 및 개발시험)

  • Byun, Young-Seop;Song, Jun-Beom;Kim, Jae-Nam;Jeong, Jin-Suk;Song, Woo-Jin;Kang, Beom-Soo
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.42 no.1
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    • pp.37-46
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    • 2014
  • This paper describes the conceptual design and development test procedure of a unmanned scaled-down personal air vehicle(PAV) with drive and flight dual mode capability. Trade studies on operational requirements led to the suggestion of a quad tilt prop platform which has nacelle tilt capability with multi rotor configuration. Motors for propeller propulsion and driving mechanism were integrated into a single nacelle, then they were implemented by nacelle tilt mechanism for conversion between the drive and the flight modes. Primary design parameters and initial specifications were confirmed through conceptual design, then functional tests were performed with the test platforms for the drive and the flight modes.

Experimental Research of Multi-Stage Axial Compressor Stability Enhancement by Air Injection (다단 축류압축기의 안정성 개선을 위한 실험적 연구)

  • Lim, Young-Cheon;Lim, Hyung-Soo;Song, Seung-Jin;Kang, Shin-Hyoung
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2009.11a
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    • pp.378-381
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    • 2009
  • A rotating stall, an instable phenomenon of compressor, brings about reducing the pressure rise, the efficiency of compressor and a mechanical demage. In order to improve instability and extend operating range, it was performed that a stability enhancement experiment applying air injection method at the 4-stage low-speed axial compressor. The coanda nozzle was used to inject air in axial direction at rotor tip and 8 injectors were set up at regular interval at the upstream of 1st stage rotor. At 80% speed, injectors were worked before rotating stall happened. As injecting the 5.4% air of mode inception flow rate, the stability of compressor operation enhanced about 4%.

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A Study on the Polarity Discrimination Method of the Stator Windings for 3 Phase Induction Motors based on the Residual Magnetism and I Winding Connection (잔류자기와 I 결선에 의한 3상유도전동기 고정자 권선의 극성판별법에 대한 연구)

  • Choi, Soon-Man
    • The Transactions of The Korean Institute of Electrical Engineers
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    • v.64 no.1
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    • pp.72-77
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    • 2015
  • When connecting 6 lead wires from stator windings to the terminals of 3 phase induction motors for Y or ${\triangle}$ connection, it is feared that the polarities of windings could be reversed each other if the wire tags are lost or erased, resulting in inadmissibly high current to motors in case of starting. To protect motors against such situations, some test procedures are necessary during wire connection which need to be easy ways to electricians without particular tools except a general multi-tester and with less time-consuming in the field. This study focuses on a test measure to satisfy these requirements which is able to provide them a convenient procedure for winding polarity discrimination considering the field condition. Here, the proposed measure utilizes the residual magnetism of the rotor and checks the indication of voltage or current at windings which are induced by the residual flux of rotor when rotating it by hands with 3 stator windings connected in the form of I connection. Principle characteristics and experiment results for this method are analyzed in the view of the effectiveness and applicability for the winding polarity discrimination.

The Unsteady Aerodynamic Characteristics of a Cascade subjected to a upstream wake with different pitch (다른 크기의 피치를 가진 후류장에 놓인 익렬의 비정상 공기역학적 특성에 관한 수치해석적 연구)

  • Jeon, H.J.;Kang, D.J.
    • Proceedings of the KSME Conference
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    • 2001.11b
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    • pp.610-615
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    • 2001
  • Effects of rotor-stator blade count ratio on the unsteady aerodynamic characteristics of a cascade was studied by using a Navier-Stokes code. Present Navier-Stokes code is a parallel code and works on a multi-cpu machine. It is based on the SIMPLE algorithm and uses QUICK scheme for convection terms and second order back difference for all temporal derivatives. Computations were carried out for two cases : case 1 is for 3 stator cascade passages subjected to two upstream wakes while case 2 is for 2 stator cascade passages subjected to three upstream wakes. Numerical solutions show that rotor-stator blade count ratio plays a significant role in the unsteady aerodynamic characteristics of the stator cascade. Case 2 shows smaller unsteady fluctuation than case 1, even if they show the same time averaged value. The smaller fluctuation of case 2 is believed due to strong interaction between unsteady vortices. The unsteady lift variation of case 2 is shown to have many high frequency fluctuations as more unsteady vortices travel around the cascade. The unsteady turbulent kinetic energy due to the upstream wake is also shown to decay faster through the cascade passage than in the free stream.

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Development and Performance Investigation on a 60kW Induction Motor for EV Propulsion

  • Chun, Yon-Do;Park, Byoung-Gun;Kim, Dong-Jun;Choi, Jae-Hak;Han, Pil-Wan;Um, Sukkee
    • Journal of Electrical Engineering and Technology
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    • v.11 no.3
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    • pp.639-643
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    • 2016
  • This paper introduces the development process and investigation of a 60kW induction motor for electric vehicles. We present performance improvement in the induction motor of electric vehicle using copper die-casting based on a multi-gate process. Copper die-casting motors can reduce the size of the motor, the loss of the rotor, and material costs. We also introduce electromagnetic, thermal, mechanical design and analysis results that satisfy the design and the performance requirements. In order to analyze losses accurately of induction motor, commercial finite element analysis is done considering PWM voltage and thermal characteristics by using lumped-circuit parameters. Experimental tests are also carried out to validate the traction motor design.

Design Optimization of Intake Muffler for Fuel Cell Electric Vehicle APU (연료전지 자동차의 공기 공급계용 흡기 소음기의 최적 설계)

  • Kim, Eui-Youl;Lee, Young-Joon;Lee, Sang-Kwon
    • Transactions of the Korean Society of Automotive Engineers
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    • v.20 no.5
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    • pp.44-52
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    • 2012
  • Fuel cell electric vehicles have some noise problems due to its air processing unit which is required to feed the ambient air into the fuel cell stack. Discrete-frequency noises are radiated from a centrifugal blower due to rotor-stator interaction. Their fundamental frequency is the blade passing frequency, which is determined by the number of rotor blades and their rotating speed. To reduce such noises, multi-chamber perforated muffler has been designed. In this paper, in order to improve the transmission loss of a perforated muffler, the relationship between the impedance model of a perforated hole and its noise reduction performance is studied, and the applicability of a short-length perforated muffler to air processing unit of fuel cell system is described using acoustic simulation results and experimental data. The acoustic velocity vector across the neck of a perforated hole is very important design factor to optimize the transmission of an intake muffler. The suggested short-length perforated muffler is effective on discrete-frequency noises while keeping the volume of intake muffler minimized.

Study on the Available Power of a Wind Turbine for Wind Farm Control (풍력단지 제어를 위한 생산가능 출력에 대한 연구)

  • Oh, Yong Oon;Paek, In Su;Nam, Yoon Su;La, Yo Han
    • Journal of the Korean Solar Energy Society
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    • v.34 no.1
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    • pp.1-7
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    • 2014
  • A study on the available power of a wind turbine to be used for wind farm control was performed in this study, To accurately estimate the available power it is important to obtain a suitable wind which represents the three dimensional wind that the wind turbine rotor faces and also used to calculate the power. For this, two different models, the equivalent wind and the wind speed estimator were constructed and used for dynamic simulation using matlab simulink. From the comparison of the simulation result with that from a commercial code based on multi-body dynamics, it was found that using the hub height wind to estimate available power from a turbine results in high frequency components in the power prediction which is, in reality, filtered out by the rotor inertia. It was also found that the wind speed estimator yielded less error than the equivalent wind when compared with the result from the commercial code.

Thermodynamic Design of J-T Neon Refrigeration System Utilizing Modified Roebuck Compression Device (변형 Roebuck 압축기를 이용한 J-T 네온 냉각시스템의 열역학적 설계)

  • 정제헌;정상권
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.15 no.5
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    • pp.432-438
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    • 2003
  • This paper describes a modified Roebuck compression device as a potential compression device of a rotating cryogenic refrigeration system in superconducting machine such as generator or motor. The conventional cryogen transfer method from stationary refrigeration system to rotating system can be eliminated by an on-board cryogenic refrigeration system that utilizes well-designed multi-stage modified Roebuck compression device. This paper shows basic thermodynamic analysis of modified Roebuck compression device and its application for compressing neon at 77 K with substantial pressure ratio when the rotor diameter is 0.8 m with rotating speed of 3600 rpm. The device does not require any moving part in rotating frame, but two separate thermal reservoirs to convert thermal energy into mechanical compression work. The high temperature thermal reservoir is atmospheric environment at 300 K and the low temperature thermal reservoir is assumed as a liquid nitrogen bath at 77 K. The concept of the compression device in this paper demonstrates its usefulness of generating high-pressure neon at 77 K for rotating J-T neon refrigeration cycle of superconducting rotor.

Design of Control Mixer for 40% Scaled Smart UAV (스마트무인기 축소모형의 조종면 혼합기 설계)

  • Gang, Yeong-Sin;Park, Beom-Jin;Yu, Chang-Seon
    • Aerospace Engineering and Technology
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    • v.5 no.2
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    • pp.240-247
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    • 2006
  • Tilt rotor aircraft is a multi-configuration airplane which has three independent flight modes; helicopter, conversion, and aiplane. The control surface mixer resign is reqctired to generate and distribute efficient control forces and moments in each flight mode. In the conversion mode, the thrust vector is changed from helicopter mode to airplane, therefore the thrust vector makes undesired forces and moments which affect on pitch, roll and yaw dynamics. This paper describes the design results of control surface mixer design which minimize the undesired forces and moments due to nacelles tilting angle change for 4O% scaled model.

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