• Title/Summary/Keyword: LCD manufacturing company

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From Printing Graphics to Printing Electronics, The Digital Revolution in Display Manufacturing

  • Elizur, Eran
    • 한국정보디스플레이학회:학술대회논문집
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    • 2007.08a
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    • pp.193-194
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    • 2007
  • In this paper we present work done by Kodak Graphic-Communications-Group and our partners demonstrating applications where laser direct imaging could replace photolithography in display manufacturing. Such applications range from direct manufacturing (e.g. LCD color-filters) to producing “masters” where manufacturing is done by traditional printing methods (e.g. flexography, Gravure-printing).

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FOS improvement through the growth speed increase of A-Si layer in TFT process

  • Kim, Pyung-Hun;Kang, I.B.;Lee, Eui-Wan;Jung, Ji-Man;Gil, W.S.;Lee, Hyung-Gi;Lee, Y.H.
    • 한국정보디스플레이학회:학술대회논문집
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    • 2004.08a
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    • pp.1040-1043
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    • 2004
  • As time goes by, the market demand increases and each LCD panel manufacturing company makes every effort to produce more panels in a limited time. It is necessary to reduce the cost and time of production for the improvement of productivity in manufacturing companies. The increased speed of thin films growth used in the TFT process brings improvement of productivity but it is also accompanied by a drop in display quality due to a characteristic change of the thin film. So in our dissertation, we deal with the increased speed of a-Si layer growth and the proportioned a drop in characteristic quality. We discuss a drop in display quality by a characteristic change of a-Si layer and we propose a counter-plan through panel design improvement. We have already applied our plan to the 15" XGA panel and confirmed the improved result.

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Auto Defect Repair Algorithm for LCD Panel Review & Repair Machine (LCD 패널 Review & Repair 장비의 결함수정 자동화 알고리즘)

  • Lee, W.C.;Lim, S.M.;Lee, S.K.;Jeong, S.H.;Hong, S.K.
    • Laser Solutions
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    • v.15 no.1
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    • pp.6-9
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    • 2012
  • In TFT-LCD manufacturing process, various defects are generated by manufacturing machine trouble or particle. These defects can be repaired through the TFT-Laser repair process that only can't be automated in TFT-LCD manufacturing Process. In this Paper, we propose auto defect algorithm for TFT-LCD laser repair machine using image processing algorithm in order to automate process. Proposed algorithm can detect very small defects (< 2um) in 98% success ratio, and generated laser repair path guarantee highly precise position accuracy. Through proposed system, much of the work still done the old-fashioned way, by hand, can be automated and manufacturing company can be strengthed the competitiveness of cost.

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An Empirical Study of Improving Total Productivity using Arena for BLU Assembly Process in LCD (LCD 부품 조립의 생산성 향상을 위한 실증적 연구)

  • Byeon, Eui-Seok;Lee, Jang-Ryong
    • Proceedings of the Korean Operations and Management Science Society Conference
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    • 2005.05a
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    • pp.80-83
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    • 2005
  • The competitiveness of the manufacturing company is evaluated in terms of line productivity, quality cost, inventory level, logistics efficiency, and so on. The productivity is defined by the number of products divided by the number of workers within the given operation time. Increasing the productivity is not easy to man-operated situation in the line, since it heavily depends on the standard time of the workers. This paper deals with the productivity of the Back Light Unit assembler for TFT-LCD, and proposes the methodology of investigating the optimal process by simulation of Arena.

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Analysis of Local Exposure Levels of Radiation Emitted from Soft X-ray Ionizers in LCD Manufacturing Processes (LCD 제조공정의 이온화 장치에 대한 전리방사선 지역노출특성 분석)

  • Kim, JoonBeom;Chung, Eun-Kyo;Jung, Kihyo
    • Journal of Korean Society of Occupational and Environmental Hygiene
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    • v.31 no.4
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    • pp.342-352
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    • 2021
  • Objectives: This study analyzed the local exposure levels of radiation emitted from the equipment with soft X-ray ionizers to investigate the radiation exposure levels in Liquid Crystal Display(LCD) manufacturing processes. Methods: This study measured the local radiation levels for the equipment installed in two LCD manufacturing companies. The equipment were installed at diverse processes and equipped with various number of ionizers. The local radiation levels were measured on the surface of the equipment by using direct reading equipment, and the measurements were converted into annual effective dose by considering the radiation exposure time of workers. Statistical analyses were performed to investigate the radiation exposure characteristics. Results: Annual effective doses for 97.6% of the equipment being measured were less than 1 mSv. However, the range of annual effective doses was 0.004 mSv ~ 2.167 mSv, which indicated a large variation among the equipment. Statistical analyses of the study found that this large variation was raised due to improper shielding of the equipment rather than process and/or equipment characteristics. To pinpoint the cause of this large variation in annual effective dose, this study improved the shielding of the equipment being radiated over 1 mSv and found that their average effective dose was reduced from 1.604 mSv to 0.126 mSv after shielding improvement. Conclusions: Relatively high exposure levels of radiation were observed in some equipment where their shielding were insufficiently thick and/or sealed. This finding implies that the shielding of the equipment is an important engineering countermeasure to control the radiation exposure levels in industries.

The design and FPGA implementation of a general-purpose LDI controller for the portable small-medium sized TFT-LCD (중소형 TFT-LCD용 범용 LDI 제어기의 설계 및 FPGA 구현)

  • Lee, Si-Hyun
    • Journal of the Korea Society of Computer and Information
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    • v.12 no.4
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    • pp.249-256
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    • 2007
  • AIn this paper, a new desist of LDI controller IC for general purpose is proposed for driving the LDI(LCD Driver Interface) controller in $4{\sim}9$ inches sized portable small-medium TFT-LCD(Thin Film Transistor addressed -Liquid Crystal Display) panel module. The designed LDI controller was verified on the FPGA(Reld Programmable Gate Array) test board, and was made the interactive operation with the commercial TFT-LCD panel successfully. The purpose of design is that it is standardized the LDI controller's operation by one LDI controller for driving all TFT-LCD panel without classifying the panel vendor, and size. The main advantage for new general-purpose LDI controller is the usage for the desist of all panel's SoG(System on a Glass) module because of the design for the standard operation. And in the previous method, it used each LDI controller for every LCD vendor, and panel size, but because a new one can drive all portable small-medium sized panel, it results in reduction of LDI controller supply price, and manufacturing cost of AV(Audio Video) board and panel. In the near future, the development of SoG IC(Integrated Circuit) for manufacturing more excellent functional TFT-LCD panel module is necessary. As a result of this research, the TFT-LCD panel can make more small size, and light weight, and it results in an upturn of domestic company's share in the world market. With the suggested theory in this paper, it expects to be made use of a basic data for developing and manufacturing for the SoG chip of TFT-LCD panel module.

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Assessment of hazardous substances and workenvironment for cleanrooms of microelectronic industry (전자산업 청정실의 작업환경 및 유해물질농도 평가)

  • Chung, Eun-Kyo;Park, Hyun-Hee;Shin, Jung-Ah;Jang, Jae-Kil
    • Journal of Korean Society of Occupational and Environmental Hygiene
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    • v.19 no.3
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    • pp.280-287
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    • 2009
  • High-tech microelectronics industry is known as one of the most chemical-intensive industries. In Korea, Microelectronics industry occupied 38% of export and 16% of working employees work in microelectronics industry. But, chemical information and health hazards of high-tech microelectronics manufacturing are poorly understood because of rapid development and its penchant for secrecy. We need to investigate on chemical use and exposure control. We Site-visits to 6 high-tech microelectronics manufacturing company which have cleanroom work using over 1,000kg organic solvents (5 semi-conductor chips and its related parts company, 1 liquid crystal display (LCD)). We reviewed their data on chemical use and ventilation system, and measured TVOCs (Total Volatile Organic Compounds) and carbon dioxide concentration. All cleanroom air passed through hepa filters to acheive low particle levels and only 1 cleanroom uses carbon filters to minimize the organic solvents exposures In TVOC screening test, Cleanroom for semi-conductor chips and its related parts company with laminar down flow system (e.g. class 1~100) showed nondetectable level of TVOCs concentration, but Cleanroom for liquid crystal display (LCD) with conventional flow system (e.g. class 1,000~10,000) showed 327 ppm as TVOCs. Acetone concentration in cleanroom for Jig cleaning, LC Injection, Sealing processes were 18.488ppm (n=14), 49.762 ppm (n=15), 8.656 ppm (n=14) as arithmetric mean. Acetone concentration in cleanroom for LCD inspection process was 40ppm (n=55) as geometric mean, where the range was 7.8~128.7ppm and weakly correlated with ventilation rate efficiency(r=0.44, p<0.05). To control organic solvents in cleanrooms, chemical and carbon filters should be installed with hepa filters. Even though their volatile organic compounds concentration was not exceed to occupational exposure limits, considering of entrance limited cleanroom environment, long-term period exposure effects and adverse health effects of cleanroom worker need further reseach.

Study on Construction of Modular Cell Line for LCD TV by Lean 6 Sigma (Lean 6 Sigma에 의한 LCD TV의 Modular Cell Line 구축에 관한 연구)

  • Jeong, Young-Kwan;Choi, Seong-Dae;Yoo, Chong-Kyu;Cheong, Seon-Hwan
    • Journal of the Korean Society of Industry Convergence
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    • v.13 no.1
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    • pp.49-54
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    • 2010
  • Lean 6 sigma has recently been used to describe a management system which combines lean management and 6 sigma. The marriage between Lean manufacturing and 6 sigma has proven to be a powerful tool for cutting waste and improving the organization operations. Time and quality are the most important metrics in improving any company's production and profit performance. lean 6 sigma is a management innovation for improving production efficiency, process quality, cost reduction, investment efficiency and customer's satisfaction. in this paper, Advanced cell line is builded the home appliance goods of the LCD TV final assembly line of domestic company line, training the multi-skilled man and controlling the production information system based on Lean 6 sigma.

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A Study on the Extremely Low Frequency Magnetic Fields Exposure Characteristics of Workers in LCD Manufacturing Process (LCD 제조공정 종사근로자의 극저주파자기장 노출특성 연구)

  • Kim, JoonBeom;Kang, Joon Hyuk;Chung, Eun-Kyo;Jung, Kihyo
    • Journal of Korean Society of Occupational and Environmental Hygiene
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    • v.32 no.1
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    • pp.10-20
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    • 2022
  • Objectives: The aim of this study is to evaluate exposure levels of the extremely low frequency magnetic fields(ELF-MF) radiated from various electric facilities in Liquid Crystal Display(LCD) manufacturing processes. Methods: This study measured the exposure levels of personal and local ELF-MF for the electronic facilities installed in two LCD manufacturing companies. Samplers were installed around workers' waist during working hours to identify personal exposure levels, and direct reading equipment were located at 3 cm, 10 cm, and 30 cm away from the surface of the electronic facilities to measure local exposure levels. Average and maximum(ceiling) values were calculated for personal and local exposure levels. Results: Average and maximum of personal exposure levels for each worker were 0.56(mean) ± 0.02(SE) µT and 6.31 ± 0.75 µT, respectively. Statistical analyses of the study found that maximum of the personal exposure levels for engineers was significantly higher than that for operators since engineers spend more time near the electronic facilities for repairing. The range of maximum personal exposure levels was 0.50 ~ 43.50 µT and its highest level was equivalent to 4.35 % of ACGIH(American Conference of Governmental Industrial Hygienists) exposure limit value(1 mT). Maximum of local exposure levels was 8.18 ± 0.52 µT and the electronic facilities with higher exposure levels were roof rail and electric panel, which were not related to direct manufacturing. The range of maximum local exposure levels was 0.60 ~ 287.20 µT and its highest level was equivalent to 28.7 % of the ACGIH exposure limit value. Lastly, the local exposure levels significantly decreased as the measurement distance from the electronic facilities increased. Conclusions: Maximum of personal and local exposure levels did not exceed the exposure limit value of ACGIH. However, it is recommended to keep the workers as far as possible from the sources of ELF-MF.

Recovery of High Purity KI Crystal from Aqueous Waste of Polarizing Film Manufacturing Process (LCD용(用) 편광(偏光)필름제조폐용액(製造廢溶液)으로부터 고순도(高純度) KI결정(結晶) 회수(回收)에 관한 연구(硏究))

  • Kim, Dae-Weon;Jang, Seong-Tae;Choi, Soon-Ryung
    • Resources Recycling
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    • v.21 no.2
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    • pp.53-58
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    • 2012
  • A laboratory study was carried out to recover KI crystals with high purity from a waste solution generated from the production of polarizing film for LCD industry. The waste solution contains 1 to 4% KI, and other impurities such as B, PVA and etc. More than 95% purity of KI crystals were produced through refining process such as vacuum evaporation and fractional crystallization. Most of B compounds and impurities were removed by concentrating the waste solution until KI content reached about 50%. The KI crystals were washed with solvents to remove most of PVA which gave result in producing 99.5% purity of crystals. The overall recovery of KI was about 90% during the concentration process.