• 제목/요약/키워드: Heat Exchange Heater

검색결과 19건 처리시간 0.021초

대용량 청정 공기 가열 장치 설계 (Design of Large Capacity Clean Air Heater)

  • 김정우;정광수;전민준;이규준
    • 한국추진공학회:학술대회논문집
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    • 한국추진공학회 2010년도 제35회 추계학술대회논문집
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    • pp.115-118
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    • 2010
  • 공기 가열 장치는 크게 연소식과 열교환식 2가지가 있으며, 본 논문은 공기를 오염시키지 않은 열교환 방식인 청정 공기 가열 장치의 설계 방법을 기술하였다. 가열 장치는 크게 연소기 (Burner), 가열로 (Furnace), 열교환기 (Heat Exchanger), 배기구로 구성되어 되며, 가열되는 공기 유량과 입/출구 온도값으로부터 가열원인 연소기의 열용량과 연소기 연료인 LNG의 소요량을 구한다. 열교환기 내부에서 연소기의 뜨거운 연소가스와 가열되는 차가운 공기간의 열매체를 통한 간접 열교환이 이루어지므로, 가열되는 공기의 입/출구 온도에서 열교환기의 용량, 크기, 작동 최대 온도를 얻을 수 있게 된다.

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재열기를 사용한 고성능 VI 사이클 열펌프의 난방 성능 특성에 관한 연구 (A Study on the Characteristics of Heating Performance of High-Performance Heat Pump with VI cycle using Re-Heater)

  • 이진국;최광환
    • 동력기계공학회지
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    • 제19권4호
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    • pp.69-75
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    • 2015
  • In this study, the characteristics of heating performance of a high-performance air-cooled heat pump with vapor-injection(VI) cycle using re-heater was investigated experimentally. Devices used in the experiment is consist of a VI compressor, condenser, oil separator, refrigerant (economizer outlet refrigerant) re-heater, economizer, evaporator. And R410A was used as a working fluid. The experiment was conducted with two cycles(cycles A and B) for investigating heating performance. In case of cycle B, heat exchange was conducted by re-heater between outlet refrigerant of compressor and suction refrigerant of the VI system(Fig.1, re-heater). But the re-heater was not used in case of cycle A. As a result of this experiment, discharge temperature of refrigerator in compressor was shown higher value, when the cycle B was conducted, because of the heat exchange between suction refrigerant of VI cycle and outlet refrigerant of compressor in the re-heater than cycle A that was not use re-heater. it means that liquid hammer and the decrement of heating performance can be decreased by using re-heater. Also, Heating coefficient of performance(COPh) was shown about 2.98 in Cycle B which was 4% higher than Cycle A and from these results, It was confirmed that the improvement of the heating performance of heat pump with VI cycle can be achieved by applying re-heater.

고온 공기 가열기 개발 현황 조사 및 고찰 (The Review and Investigation of High Temperature Heater Development)

  • 김정우;이정민
    • 한국추진공학회지
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    • 제20권5호
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    • pp.90-98
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    • 2016
  • 극초음속 공기 흡입 추진기관의 지상 시험 시 추진기관의 고속 비행 조건을 모의하기 위해 고온 공기를 공급할 수 있는 고온 공기 가열기가 필요하다. 본 논문에서는 다양한 고온 가열기들을 조사하여 유형별로 정리하고, 장단점을 비교하였다. 가열기는 크게 유동장 내 연소 가열기, 아크 가열기, 축열식 가열기, 열교환식 가열기 4종류로 분류할 수 있었으며, 각각의 장단점이 다양하므로 목적에 맞게 가열기를 선정하여야 한다.

EXHAUST GAS HEAT RECOVERY SYSTEM FOR PLANT BED HEATING IN GREENHOUSE PRODUCTION

  • Kim, Y.J.;Ryou, Y.S.;Rhee, K.J.;Kang, G.C.
    • 한국농업기계학회:학술대회논문집
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    • 한국농업기계학회 2000년도 THE THIRD INTERNATIONAL CONFERENCE ON AGRICULTURAL MACHINERY ENGINEERING. V.III
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    • pp.639-646
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    • 2000
  • Hot air heater with light oil combustion is the most common heater for greenhouse heating in the winter season in Korea. However, since the heat efficiency of the heater is about 80%, considerable unused heat in the form of exhaust gas heat discharges to atmosphere. In order to capture this exhaust gas heat a heat recovery system for plant bed heating in the greenhouse was built and tested in the hot air heating system of greenhouse. The system consists of a heat exchanger made of copper pipes, ${\phi}\;12.7{\times}0.7t$ located inside the rectangular column of $330{\times}330{\times}900mm$, a water circulation pump, circulation plastic pipe and a water tame The total heat exchanger area is $1.5m^2$, calculated considering the heat exchange amount between flue gas and water circulated in the copper pipes. The system was attached to the exhaust gas path. The heat recovery system was designed as to even recapture the latent heat of flue gas when exposing to low temperature water in the heat exchanger. According to performance test it can recover 45,200 to 51,000kJ/hr depending on the water circulation rates of 330 to $690{\ell}$/hr from the waste heat discharged. The exhaust gas temperature left from the heat exchanger dropped to $100^{circ}C$ from $270^{circ}C$ by the heat exchange between the water and the flue gas, while water gained the difference and temperature increased to $38^{circ}C$ from $21^{circ}C$ at the water flow rate of $690{\ell}$/hr. And, the condensed water amount varies from 16 to $43m{\ell}$ at the same water circulation rates. This condensing heat recovery system can reduce boiler fuel consumption amount in a day by 34% according to the feasibility study of the actual mimitomato greenhouse. No combustion load was observed in the hot air heater.

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히트파이프를 이용한 온풍난방기 배기열회수 시스템의 열회수 특성 (Heat Recovery Characteristics of the Exhaust Heat Recovery System with Heat Pipe Unit Attached to the Hot Air Heater in the Greenhouse)

  • 강금춘;김영중;유영선;백이;이건중
    • Journal of Biosystems Engineering
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    • 제26권5호
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    • pp.441-448
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    • 2001
  • Hot air heater with light oil combustion is used as the most common heater for greenhouse heating in the winter season. However, exhaust gas heat discharged to atmosphere through chimney reaches up to 10~20% of total heat capacity of the oil burred. In order to recover the heat of this exhaust gas and to use for greenhouse heating, the heat pipe type exhaust heat recovery system was manufactured and tested in this experiment. The system consisted of a heat exchanger made of heat pipes, ø15.88${\times}$600mm located in the rectangular box of 675(L)${\times}$425(W)${\times}$370(H)mm, an air suction fan and air ducts. The number of heat pipe was 60, calculated considering the heat exchange amount between exhaust gas and air and heat transfer capacity of a heat pipe. The working fluid of heat pipe was acetone because acetone is known for its excellent heat transfer capacity. The system was attached to the exhaust gas path. According to the performance test it could recover 53,809 to 74,613kJ/h depending on the inlet air temperature of 12 to -12˚at air flow rate of 1.100㎥/h. The temperature of the exhaust gas left the heat exchanger dropped to 100$^{\circ}C$ from 270$^{\circ}C$ after the heat exchange between the suction air and the exhaust gas.

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태양열과 재열기를 사용한 VI heat pump의 성능 특성에 관한 연구 (Heating Performance Characteristics of Heat Pump with VI cycle using Re-Heater and Solar-Assisted)

  • 이진국;최광환
    • 한국태양에너지학회 논문집
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    • 제35권6호
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    • pp.25-33
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    • 2015
  • In this study, heating performance of the air-cooled heat pump with vapor-injection (VI) cycles, re-heater and solar heat storage tank was investigated experimentally. Devices used in the experiment were comprised of a VI compressor, re-heater, economizer, variable evaporator, flat-plate solar collector for hot water, thermal storage tank, etc. As working fluid, refrigerant R410A for heat pump and propylene glycol (PG) for solar collector were used. In this experiment, heating performance was compared by three cycles, A, B and C. In case of Cycle B, heat exchange was conducted between VI suction refrigerant and inlet refrigerant of condenser by re-heater (Re-heater in Fig. 3, No. 3) (Cycle B), and Cycle A was not use re-heater on the same operating conditions. In case of Cycle C, outlet refrigerant from evaporator go to thermal storage tank for getting a thermal energy from solar thermal storage tank while re-heater also used. As a result, Cycle C reached the target temperature of water in a shorter time than Cycle B and Cycle A. In addition, it was founded that, as for the coefficient of heating performance($COP_h$), the performance in Cycle C was improved by 13.6% higher than the performance of Cycle B shown the average $COP_h$ of 3.0 and by 18.9% higher than the performance of Cycle A shown the average $COP_h$ of 2.86. From this results, It was confirmed that the performance of heat pump system with refrigerant re-heater and VI cycle can be improved by applying solar thermal energy as an auxiliary heat source.

선박연료 가열용 250KW급 판형 IoT 전기히터의 기초연구 (Basic Study on 250KW-class IoT Electric Heater for Ship Fuel Heating)

  • 장성철
    • 사물인터넷융복합논문지
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    • 제7권3호
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    • pp.63-68
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    • 2021
  • 국내의 전기히터 제조업체에서는 기존 제품의 효율을 향상시키는 기술 개발에 집중하고 있다. 선박 연료용 전기히터는 그 크기가 크고 소형화/고효율화에 대한 난이도가 높아 아직까지 기술개발을 시도하는 기업은 많지 않은 실정이다. 기존의 전기히터는 선박 엔진 연료의 유동경로가 단조롭기 때문에 가열매체의 열교환 튜브와의 접촉시간이 매우 짧아 가열 효율이 낮은 구조이며, 관형으로 제작되어 있기 때문에 가열효율과 무관하게 부피가 매우 크게 제작되므로 가열장치의 설치공간을 확보해야 한다. 이로인해 해외 선진사에서 적용하고 있는 관형 전기히터 장치는 내부의 특정부분이 손상되었을때 관형 가열기를 모두 분해하여야 하고, 열교환 튜브가 손상된 경우에는 열교환 튜브를 모두 분해해야 하므로 유지와 보수에 어려움이 있다. 본 연구에서는 250kW 용량급 판형 전기히터 가열기를 통해 시간당 10ton의 선박 엔진 연료를 가열할 수 있고, 최대온도를 150℃까지 설정할 수 있는 판형 전기히터에 대한 기초연구를 수행하였다.

Heat Transfer Performance of Plate Type Absorber with Surfactant

  • Yoon, Jung-In;M. M. A. Sarker;Moon, Choon-Geun
    • Journal of Advanced Marine Engineering and Technology
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    • 제28권2호
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    • pp.243-251
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    • 2004
  • Absorption chiller/heater can utilize the unused energy of the daily life waste heat, the industry waste heat. the solar energy and the earth energy. These can contribute to energy savings. But the absorption chiller/heater has a demerit that the size of absorption chiller/heater is larger than that of the vapor compression type based on same capacity. In this study. the experimental apparatus of an absorber is manufactured as a plate. which is newly applied in an absorber. The experimental apparatus is composed of a plate type absorber. which can increase the heat exchange area per unit volume and thus facilitating to deeply investigate more detail features instead of that done by the existing type. i.e.. horizontal tube bundle type. The characteristics of heat transfer and refrigeration capacity are studied experimentally. The absorption enhancement by using surfactant is closely examined through the experiment and comparative figures are presented in quantitative and qualitative analysis.

다공형 전열판의 회전에 의한 열교환시스템의 성능에 관한 연구(Ⅰ) - 환기측과 외기측의 풍량 변화에 대하여 - (Study on the Performance of Total Heat Exchanger with Rotating Porous Plates)

  • 조동현;임태우
    • 동력기계공학회지
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    • 제9권4호
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    • pp.11-17
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    • 2005
  • This paper reports an experimental study on the performance evaluation of air-to-air heat exchanger with rotary type newly developed in this study. Air flow rate is varied from 10 to 120 m3/h. The range of RPM of the porous rotating discs mounted inside the heat exchanger unit is 0 to 50. The temperature of the return air side is set by adjusting heat supply at heater. The material of the porous rotating discs is cooper and its thickness is 1.0 mm. The heat transfer rate increased with the increase in air flow rate. It was found that the heat transfer rate, as the temperature of the return air side was increased, was improved due to higher temperature difference. The heat exchange performance increased with the increase in the temperature of the return air side at the conditions of the same RPM. The sensible heat exchange efficiency was maximum 68 to 76 percent, and enthalpy exchange efficiency 64 to 74 percent.

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온풍난방기의 배기열을 이용한 지중 난방용 온수공급시스템의 열회수특성 (Heat Recovery Characteristics of the Hot Water Supply System with Exhaust Heat Recovery Unit Attached to the Hot Air Heater for Plant Bed Heating in the Greenhouse)

  • 김영중;유영선;장진택;강금춘;이건중;신정웅
    • Journal of Biosystems Engineering
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    • 제25권3호
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    • pp.221-226
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    • 2000
  • Hot air heater with light oil burner is the most common heater for greenhouse heating in the winter season in Korea. However, since the thermal efficiency of the heater is about 80∼85%, considerable unused heat amount in the form of exhaust gas heat discharges to atmosphere. In order to capture this exhaust heat a heat recovery system for plant bed heating in the greenhouse was built and tested in the hot air heating system of greenhouse. The heat recovery system is made for plant bed or soil heating in the greenhouse. The system consisted of a heat exchanger made of copper pipes, ${\Phi}12.7{\times}0.7t$ located in the rectangular column of $330{\times}330{\times}900mm$, a water circulation pump, circulation plastic pipe and a water tank. The total heat exchanger area is 1.5$m^2$, calculated considering the heat exchange amount between flue gas and water circulated in the copper pipes. The system was attached to the exhaust gas path. The heat recovery system was designed as to even recapture the latent heat of flue gas when exposing to low temperature water in the heat exchanger. According to the performance test it could recover 45,200 to 51,000kJ/hr depending on the water circulation rates of 330 to $690\ell$/hr from the waste heat discharged. The exhaust gas temperature left the heat exchanger dropped to $100^{\circ}C$ from $270^{\circ}C$ by the heat exchange between the water and the flue gas, while water gained the difference and temperature increased to $38^{\circ}C$ from $21^{\circ}C$ at the water flow rate of $690\ell$/hr. By the feasibility test conducted in the greenhouse, the system did not encounter any difficulty in operations. And, the system could recover 220,235kJ of exhaust gas heat in a day, which is equivalent of 34% of the fuel consumption by the water boiler for plant bed heating of 0.2ha in the greenhouse.

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