• Title/Summary/Keyword: Gasification reaction

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Study on characteristics of compression and transportation of syngas produced from gasification process of high-calorific waste and Sewage Sludge (고발열량폐기물 및 탈수슬러지 혼합가스화를 통해 생산된 합성가스 압축, 이송 운전 특성)

  • Park, Soo-Nam;Ku, Jae-Hoi
    • 한국신재생에너지학회:학술대회논문집
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    • 2009.06a
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    • pp.832-835
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    • 2009
  • 폐기물의 감량화 및 자원화 기술 중 가장 대표적인 기술로 폐기물의 가스화 용융 기술을 들 수 있다. 폐기물 가스화 용융 기술은 폐기물 내의 탄소 및 수소 성분은 가스화 하여 CO, $H_2$가 주성분인 합성가스(synthesis gas, syngas)로 전환하고, 불연물은 용융하여 환경적으로 무해한 슬래그 또는 금속으로 회수하는 기술이다. 본 연구에서는 고발열량폐기물과 탈수슬러지 혼합가스화를 통하여 생산된 합성가스를 합성가스 압축기를 통하여 유용한 원료물질을 제조하는 공정인 수성가스 전환 반응(water gas shift reaction)과 가스화 반응기의 보조연료로 투입하기 위한 합성가스 압축, 이송 시스템의 운전 특성을 고찰하였다. 그 결과 고발열량폐기물과 탈수슬러지 혼합가스화에서 합성가스는 안정적으로 발생하였으며, 합성가스 압축, 이송시스템을 위한 정제설비에서의 분진제거는 99.07 %의 효율을 얻었고, 또한 합성가스 재순환 장치의 성능시험을 통하여 대기 중의 산소가 유입이 안 되는 기밀성을 확인하였다. 합성가스 압축, 이송 공급 유량 제어 실험 결과로는 합성가스 압축기 기동 시 합성가스 압축압력과 공급유량은 비례적으로 증감하는 것을 알 수 있었다.

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SNG Production Process Study in the gasification system with various feedstock (석탄, 석탄 촤, 바이오매스 등의 고체시료 가스화 반응을 통해 발생된 합성가스를 이용한 SNG 제조공정 연구)

  • Kim, Su-Hyun;Yoo, Young-Don;Kim, Mun-Hyun;Kim, Na-Rang;Kim, Hyung-Taek
    • 한국신재생에너지학회:학술대회논문집
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    • 2007.06a
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    • pp.779-783
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    • 2007
  • 본 연구에서는 가스화공정과 수성가스 전환공정, $CO_2$ 분리공정, 메탄화 공정을 주요 구성으로 한 대체(또는 합성)천연가스(SNG, Substitute or Synthetic Natural Gas)제조공정을 대상으로 석탄, 석탄 촤, 바이오매스 등의 다양한 고체시료를 적용하였을 경우 각 시료의 가스화 반응을 통해 얻어진 합성가스를 이용한 SNG 제조 공정 특성을 파악하고자 하였다. 석탄, 석탄 촤, 바이오매스를 적용한 SNG 공정해석 결과 가스화 공정, 수성가스 전환 공정, 메탄화 공정의 운전 용도가 각 800도, 450도, 300도이고, 수성가스 전환 공정 출구의 합성가스 $H_2$/CO ratio(mol basis)가 3인 조건에서 SNG/Feed ratio는 석탄, 석탄 촤, 바이오매스가 각각 0.35, 0.34, 0.08로 나타났고. SNG Efficiency(%) 는석탄, 석탄 촤 바이오매스에 대해서 각각 61.2%. 48.2%, 17.5%로 나타났다. 또한, 석탄 촤를 대상으로 가스화 공정에서의 산화제 투입 조건 및 스팀 투입조건의 변화에 따른 합성가스 발생 특성을 살펴보았다.

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Estimation of Synthesis Gas Composition by Biomass Fuel Conditions using Thermodynamic Equilibrium Model (열역학적 평형모델을 이용한 바이오매스 연료조건에 따른 합성가스 조성의 예측)

  • Hong, Seong-Gu
    • Journal of The Korean Society of Agricultural Engineers
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    • v.57 no.1
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    • pp.79-87
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    • 2015
  • A thermochemical equilibrium model was constructed for predicting composition of synthesis gas in biomass gasification. The model included estimation of equilibrium constants using Gibbs free energy. After constructing the model, the results were compared with the experimental values and predictions from a previous model. Gas compositions were reasonably well agreed with them and showed effects of operational and fuel condition. When the reaction temperature increased, the lower heating values decreased due to the decrease in CH4 concentrations. The methane concentrations were lower than those observed in experimental results. The model was used to predict the gas composition and heating values for the cases of mixed fuel of charcoal and un-dry woodchips. Although downdraft gasifiers require fuels less than 15% of moisture contents, the model results indicated that the mixed fuel with charcoal and woodchips which had over 25% of moisture contents could be used in the downdraft gasifiers. It might be explained by increase in energy density resulting from mixing charcoal. The results imply that the efforts and costs for drying biomass fuels could be reduced by mixing charcoal or fuels with higher calorific values.

Study of Kinetics for Removal H2S by Natural Manganese ore Sorbent (황화수소 제거를 위한 천연망간광석 탈황제의 반응 속도 연구)

  • Yoon, Yeo Il;Kim, Myung Wook;Kim, Sung Hyun
    • Clean Technology
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    • v.7 no.3
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    • pp.187-194
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    • 2001
  • The desulfurization process which belongs to the gas refining part is the unit process that eliminates $H_2S$ and COS in the coal gas formed by the coal gasification part in the integrated gasification combined cycle(IGCC). In this study, natural manganese ores were selected as the raw material of the desulfurization sorbent due to economical efficiency. Initial rates for the reactions between $H_2S$ and desulfurization sorbent using natural manganese ores were determined in a temperature range of $400{\sim}800^{\circ}C$ using a thermobalance reactor. All reactions were first order with respect to $H_2S$ and were in accord with the Arrhenius equations. When sulfidation reaction was controlled by diffusion, the temperature dependence of the effective diffusivity was given by the Arrhenius equation. Activation energies and frequency factors were obtained from the product layer diffusion coefficient of various sorbents by plotting as Arrhenius equation form.

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Experimental study on the characteristics of Vacuum residue gasification in an entrained-flow gasifier (습식 분류상 가스화장치를 이용한 중질잔사유(Vacuum residue)의 가스화 특성연구)

  • ;;;;;;;A. Renevier
    • Proceedings of the Korea Society for Energy Engineering kosee Conference
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    • 2002.11a
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    • pp.171-184
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    • 2002
  • Approx. 200,000 bpd vacuum residue oil is produced from oil refineries in Korea. These are supplying to use asphalt, high sulfur fuel oil, and upgrading at the residue hydro-desulfurization unit. Vacuum residue oil has high energy content, however high sulfur content and high concentration of heavy metals represent improper low grade fuel. To meet growing demand for effective utilization of vacuum residue oil from refineries, recently some of the oil refinery industries in Korea, such as SK oil refinery and LG Caltex refinery, have already proceeded feasibility study to construct 435-500 MWe IGCC power plant and hydrogen production facilities. Recently, KIER(Korea Institute of Energy Research) are studing on the Vacuum Residue gasification process using an oxygen-blown entrained-flow gasifier. The experiment runs were evaluated under the reaction temperature : 1,100~1,25$0^{\circ}C$, reaction pressure : 1~6kg/$\textrm{cm}^2$G, oxygen/V.R ratio : 0.8~0.9 and steam/V.R ratio : 0.4-0.5. Experimental results show the syngas composition(CO+H$_2$) : 85~93%, syngas flow rate : 50~110Mm$^3$/hr, heating value : 2,300~3,000 ㎉/Nm$^3$, carbon conversion : 65~92, cold gas efficiency : 60~70%. Also equilibrium modeling was used to predict the vacuum residue gasification process and the predicted values were compared reasonably well with experimental data.

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Experimental Study on the Characteristics of Vacuum Residue Gasification in an Entrained-flow Gasifier (습식 분류상 가스화장치를 이용한 중질잔사유(Vacuum Residue)의 가스화 특성연구)

  • ;;;;;;;A. Renevier
    • Journal of Energy Engineering
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    • v.12 no.1
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    • pp.49-57
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    • 2003
  • Approx. 200.000 bpd vacuum residue oil is produced from oil refineries in Korea, and is supplied to use asphalt, high sulfur fuel oil and for upgrading at the residue hydro-desulfurization unit. Vacuum residue oil has high energy content, however its high sulfur content and high concentration of heavy metals represent improper low grade fuel. To meet growing demand for effective utilization of vacuum residue oil from refineries, recently some of the oil refinery industries in Korea, such as SK oil refinery and LG Caltex refinery, have already proceeded feasibility study to construct 435~500 MWe IGCC power plant and hydrogen production facilities. Recently, KIER (Korea Institute of Energy Research) are studying on the Vacuum Residue gasification process using an oxygen-blown entrained-flow gasifier. The experiment runs were evaluated under the reaction temperature: 1.100~l,25$0^{\circ}C$, reaction pressure: 1~6 kg/$\textrm{cm}^2$G, oxygen/V.R ratio: 0.8~0.9 and steam/V.R ratio: 0.4~0.5. Experimental results show the syngas composition (CO+H$_2$): 85~93%, syngas flow rate: 50~l10 Nm$^3$/hr, heating value: 2,300~3,000 k㎈/Nm$^3$, carbon conversion: 65~92, cold gas efficiency: 60~70%. Also equilibrium modeling was used to predict the vacuum residue gasification process and the predicted values were compared reasonably well with experimental data.

Pyrolytic Gasification Characteristics of Waste Tires and Waste Synthetic Resins (폐타이어 및 폐합성수지류의 건류가스화 특성)

  • 노남선;김광호;신대현;김동찬
    • Resources Recycling
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    • v.9 no.1
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    • pp.27-35
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    • 2000
  • Characteristics of pyrolytic gasification were examined for the waste tire and 7 types of waste synthetic resin, using a bench scale experimental facility. the product gas temperature of waste tires was $150~300^{\circ}C$ and the temperature profile in the combustion zone of the lower reactor part tended to be clearly distinguished from that in the gasification zone of the upper part. However, in the case of waste synthetic resins, there were no clear distinction and temperature fluctuation was severe, depending on the reaction time. Product gas quantity, which depends on that of supplied (1st) air, was found to be 105~135% of the 1st air amount at the steady state. The concentration of noncombustible components in product gas was 80~90 vol.% and the high heating value of the product gas calculated from gas compositions was 1,500~3,000 kcal/N㎥ for waste tire, and 300~2,900 kcal/N㎥ for waste synthetic resins, respectively. Heating value of product gas and combustible gas concentration were increased in proportion to 1st air amount when 1st air amount is below $0.35N\textrm{m}^3$/min.

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Effect of Flow Distribution on the Combustion Efficiency In an Entrained-Bed Coal Reactor (분류층 석탄반응로에서 유동분포가 연소성능에 미치는 영향)

  • CHO, Han Chang;SHIN, Hyun Dong
    • Transactions of the Korean Society of Mechanical Engineers B
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    • v.23 no.8
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    • pp.1022-1030
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    • 1999
  • A numerical study was carried out to analyze the effect of flow distribution of stirred part and plug flow part on combustion efficiency at the coal gasification process in an entrained bed coal reactor. The model of computation was based on gas phase eulerian balance equations of mass and momentum. The solid phase was described by lagrangian equations of motion. The $k-{\varepsilon}$ model was used to calculate the turbulence flow and eddy dissipation model was used to describe the gas phase reaction rate. The radiation was solved using a Monte-Carlo method. One-step parallel two reaction model was employed for the devolatilization process of a high volatile bituminous Kideco coal. The computations agreed well with the experiments, but the flame front was closer to the burner than the measured one. The flow distribution of a stirred part and a plug flow part in a reactor was a function of the magnitude of recirculation zone resulted from the swirl. The combustion efficiency was enhanced with decreasing stirred part and the maximum value was found around S=1.2, having the minimum stirred part. The combustion efficiency resulted from not only the flow distribution but also the particle residence time through the hot reaction zone of the stirred part, in particular for the weak swirl without IRZ(internal recirculation zone) and the long lifted flame.

Water Gas Shift reaction research of the synthesis gas for a hydrogen yield increase (수소 수율 증가를 위한 합성가스의 수성가스전환 반응 연구)

  • Kim, Min-Kyung;Kim, Jae-Ho;Kim, Woo-Hyun;Lee, See-Hoon
    • 한국신재생에너지학회:학술대회논문집
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    • 2009.06a
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    • pp.840-843
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    • 2009
  • 폐자동차의 최종처분 과정에서 발생하는 자동차 파쇄 폐기물(Automobile Shredder Dust)은 대부분이 고분자 화합물로 높은 발열량을 가지고 있다. 또한 할로겐족 원소가 포함된 난연성 고분자류가 많아 다이옥신의 생성 우려가 높은 고분자류와 다이옥신 생성의 촉매 역할을 할 수 있는 금속성분이 많이 함유되어 있어 가스화용융시스템에 적용하여 처리하기에 매우 적합한 폐기물이다. 본 연구에서는 ASR의 가스화 용융 시설에서 고농도 CO를 함유한 합성가스를 수성가스전환반응(Water Gas Shift reaction, WGS)을 이용하여 수소의 수율을 높이는 기술을 제시하였다. 가스화 용융 설비에서 배출되는 합성가스 조성을 기준으로 적합한 고정층 WGS 반응기를 설계하고, 고온 촉매(KATALCO 71-5M)와 저온 촉매(KATALCO 83-3X)를 사용하여 실험하였다. 수성가스 반응 후의 가스 조성은 온도가 상승할수록 일산화탄소가 줄어들고 이에 따라 수소와 이산화탄소 발생량이 증가 되어 고온 촉매를 사용했을 경우 일산화탄소 전환율 ($1-CO_{out}/CO_{in}$)은 55.6에서 95.8%까지 상승하였다. 동일한 온도조건에서는 촉매에 관계없이 $CO/H_2$가 감소할수록 전환율도 감소하는 경향을 보였지만 동일한 합성가스 조성에서 일산화탄소 전환율을 비교하면 저온 촉매가 고온 촉매보다 매우 우수함을 알 수 있었다.

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Corrosion of Alumina-Chromia Refractories by Alkali Vapors; II. Experimenal Approach

  • Lee, Kyung-Ho;Jesse . Brown Jr
    • The Korean Journal of Ceramics
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    • v.1 no.2
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    • pp.86-90
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    • 1995
  • Theoretical predictions for thermodynamically stable phases which formed when alkali(sodium and potassium) vapors reacted with alumina-chromia refractories under coal gasifying atmosphere were confirmed experimentally using a laboratory-scale coal gasifying reaction system and a commercial alumina-chromia refractory using SEM, XRD, and EDAX. Alkali concentration profiles in the refractory as a function of time were also determined. The results showed that the compounds that formed were $X_2O{\cdot}Al_2O_3, X_2O{\cdot}Cr_2O_3, X_2O{\cdot}5Al_2O_3, X_2O{\cdot}7Al_2O_3, X_2O{\cdot}11Al_2O_3(X=Na^+ \;or\; K^+)$, depending upon the alkali concentration and time of exposure at high temperatures. The presence of sulfur in gasifying atmospheres did not appear to affect the alkali reaction produces. Alkali pentration into the alumina-chromia refractory was deep and the formation of the $Na_2O{\cdot}Al_2O_3/K_2O{\cdot}Al_2O_3$ compunds resulted in the serious deformation of the refractory due to the large volume expansion at the reaction surface. The hot face of the alumina-chromia refractory in service under an alkali environment is prone to failure by alkali attack.

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