• Title/Summary/Keyword: Bubble volume concentration

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Evaluation of Flotation Efficiency and Particle Separation Characteristics of Carbon Dioxide Bubbles using Collision Efficiency Model (단일포집자충돌(SCC) 모델을 이용한 이산화탄소기포의 입자분리특성과 부상효율 평가)

  • Lee, Jun-Young;Kim, Seong-Jin;Yoo, Young-Hoon;Chung, Paul-Gene;Kwon, Young-Ho;Park, Yang-Kyun;Kwak, Dong-Heui
    • Journal of Korean Society on Water Environment
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    • v.28 no.1
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    • pp.129-136
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    • 2012
  • In this century, scientists realized that carbon dioxide gas in the atmosphere cause a greenhouse effect which affects the planet's temperature. Therefore lots of attempts have carried out to decrease the discharge of carbon dioxide gas in the field. The dissolved carbon dioxide flotation (DCF) process was developed as an alternative of DAF process to decrease the discharge and reuse of carbon dioxide as well as to save energy consumption. To investigate the particle separation characteristics and the flotation efficiency of carbon dioxide, SCC model was employed in the DCF process which has been applied extensively for the evaluation and simulation in the DAF process. The simulation results by the SCC model revealed the predicted curve of flotation efficiency became decreased gradually over the optimal pressure range of saturator about 1.6 atm in accordance with the experiment results of the DCF pilot plant and the size distribution and the bubble volume concentration of $CO_{2}$ bubbles depending on the operation pressure of saturator. The findings through the simulation results led to the conclusion that there was no significant difference between $CO_{2}$ bubbles and air bubbles, affecting on the practical flotation efficiency, in terms of the initial collision and attachment efficiency.

Treatment Characteristics and Application of DAF Process for Effective Solid Separation in BNR Municipal Wastewater Treatment System (BNR 하수처리시스템에서 효과적 고형물 분리를 위한 DAF 공정의 적용과 처리특성)

  • Kwak, Dong-Heui;Rhu, Dae-Hwan
    • Journal of Korean Society of Water and Wastewater
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    • v.24 no.3
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    • pp.267-276
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    • 2010
  • Many plants have been improved to adapt the target of the biological treatment processes changed from organics to nutrients since the water quality criteria of effluent was reinforced and included T-N and T-P for the municipal wastewater treatment plant. To meet the criteria of T-N and T-P, the conventional biological reactor such as aeration tank in activated sludge system is changed to the BNR (biological nutrient removal) processes, which are typically divided into three units as anaerobic, anoxic and oxic tank. Therefore, the solid separation process should be redesigned to fit the BNR processes in case of the application of the DAF (dissolved air flotation) process as an alternatives because the solid-liquid separation characteristics of microbial flocs produced in the BNR processes are also different from that of activated sludge system as well. The results of this study revealed that the microbial floc of the anaerobic tank was the hardest to be separated among the three steps of the unit tanks for the BNR processes. On the contrary, the oxic tank was best for the removal efficiency of nutrients as well as suspended solid. In addition, the removal efficiency of nutrients was much improved under the chemical coagulation treatment though coagulation was not indispensable with a respect to the solid separation. On the other hand, in spited that the separation time for the microbial floc from the BNR processes were similar to the typical particles like clay flocs, over $2.32{\times}10^3$ ppm of air volume concentration was required to keep back the break-up of the bubble-floc agglomerates.

Thickening of Sludge from DAF process by Flotation; Application of Solid Flux Theory and Effective Factors (DAF 슬러지의 부상식 농축; 고형물 플럭스법 적용과 영향인자)

  • Park, Sangcheol;Han, Mooyoung;Dockko, Seok;Kwon, Soonbuhm
    • Journal of Korean Society of Water and Wastewater
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    • v.20 no.4
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    • pp.617-626
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    • 2006
  • Compared with the sludge from gravity sedimentation, it is difficult for operations to settle the sludge occurred from dissolved-air-flotation (DAF). Even though there are some problems in treating DAF sludge with conventional gravity thickeners, those has been used until now. In this study, Solid Flux theory for gravity thickening was applied to the Solid Flux of DAF sludge through flotation in order to develop new methodology for treatment of DAF sludge. Also, characteristics of DAF sludge were investigated. From the experiment results, it was revealed that the higher the polymer dosage, at fixed the solid concentration, the greater the rising velocity becomes. When we applied solid flux theory, the relationship, which is similar to that of gravity thickening, has been achieved. Also, we could find the proper polymer dosage from the rising velocity is about 50 mg/L. Consequently, the limiting solid flux can be derived from the relationship between the total solid flux and the withdrawal velocity of DAF sludge. Furthermore, the factors, such as solid concentrations, bubble volume, pH, zeta potential, and temperature, have effects on the flotation and sedimentation for DAF sludge treatment.

Boiling Heat Transfer Coefficients of Nanofluids Using Carbon Nanotubes (탄소나노튜브를 적용한 나노유체의 비등 열전달계수)

  • Lee, Yo-Han;Jung, Dong-Soo
    • Journal of the Korean Solar Energy Society
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    • v.29 no.5
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    • pp.35-44
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    • 2009
  • In this study, boiling heat transfer coefficients(HTCs) and critical heat flux(CHF) are measured on a smooth square flat copper heater in a pool of pure water with and without carbon nano tubes(CNTs) dispersed at $60^{\circ}C$. Tested aqueous nanofluids are prepared using multi-walled CNTs whose volume concentrations are 0.0001, 0.001, 0.01, and 0.05%. For dispersion of CNTs, polyvinyl pyrrolidone(PVP) is used in distilled water. Pool boiling HTCs are taken from $10kW/m^2$ to critical heat flux for all nanofluids. Test results show that the pool boiling HTCs of the nanofluids are lower than those of pure water in entire nucleate boiling regime. On the other hand, critical heat flux is enhanced greatly showing up to 200% increase at volume concentration of 0.001% CNTs as compared to that of pure water. This is related to the change of surface characteristics by the deposition of CNTs. This deposition makes a thin CNT layer on the surface and the active nucleation sites of heat transfer surface are decreased due to this layer. The thin layer acts as the thermal resistance and also decreases the bubble generation rate resulting in a decrease in pool boiling HTCs. The same layer, however, maintains the nucleate boiling even at very high heat fluxes and reduces the formation of large vapor canopy at near CHF resulting in a significant increase in CHF.

Comparative Study on Removal Characteristics of Disinfection By-products by Air Stripping and Flotation Processes (탈기와 부상 공정에 의한 소독부산물의 제거특성에 관한 비교 연구)

  • Cha, Hwa-Jeong;Won, Chan-Hee;Lee, Kang-Hag;Oh, Won-Kyu;Kwak, Dong-Heui
    • Journal of Korean Society of Environmental Engineers
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    • v.38 no.9
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    • pp.513-520
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    • 2016
  • It is well known that volatile compounds including disinfection by-products as well as emissive dissolved gas in water can be removed effectively by air stripping. The micro-bubbles of flotation unit are so tiny as microns while the diameter of fine bubbles applied to air stripping is ranged from hundreds to thousands of micrometer. Therefore, the micro-bubbles in flotation can supply very wide specific surface area to transfer volatile matters through gas-liquid boundary. In addition, long emission time also can be gained to emit the volatile compound owing to the slow rise velocity of micro-bubbles in the flotation tank. There was a significant difference of the THMs species removal efficiency between air stripping and flotation experiments in this study. Moreover, the results of comparative experiments on the removal characteristics of THMs between air stripping and flotation revealed that the mass transfer coefficient, $K_La$ showed obvious differences. To overcome the limit of low removal efficiency of dissolved volatile compounds such as THMs in flotation process, the operation range of bubble volume concentration is required to higher than the operation condition of conventional particle separation.

Sensitivity Analysis of Initial Pressure and Upper Control Limit on the Pressure Decay Test for Membrane Integrity Evaluation (압력손실시험을 이용한 막 완결성 평가에서 초기압력 및 UCL 도출인자 민감도 분석)

  • Lee, Joohee;Hong, Seungkwan;Hur, Hyunchul;Lee, Kwangjae;Choi, Youngjune
    • Journal of Korean Society on Water Environment
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    • v.24 no.6
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    • pp.793-800
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    • 2008
  • Recently domestic drinking water industry has recognized membrane-based technology as a promising alternative for water treatment. To ensure successful application of membrane processes, the integrity of membrane systems should be maintained. According to US EPA guidance, the pressure decay test based on the bubble point theory is recommended to detect any membrane defection of which size is close to the smallest diameter of Cryptosporidium oocysts, $3{\mu}m$. Proper implementation of the pressure decay test is greatly affected by initial test pressure, and the interpretation of the test results is associated with upper control limit. This study is conducted to investigate various factors affecting determination of initial test prtessure and upper control limit, including membrane-based parameters such as pore shape correction factor, surface tension and contact angle, and system-based parameters, such as volumetric concentration factor and total volume of system. In this paper, three different hollow fibers were used to perform the pressure decay test. With identical initial test pressure applied, their pressure decay tendency were different from each other. This finding can be explained by the micro-structure disparity of those membranes which is verified by FESEM images of those membranes. More specifically, FESEM images revealed that three hollow fibers have asymmetry, deep finger, shallow finger pore shape, respectively. In addition, sensitivity analysis was conducted on five parameters mentioned above to elucidate their relation to determination of initial test pressure and upper control limit. In case of initial pressure calculation, the pore shape correction factor has the highest value of sensitivity. For upper control limit determination, system factors have greater impact compared to membrane-based parameters.

Study to enhance the settleability of deep aeration tank MLSS (Mixed Liquor Suspended Solid) by air sparging (탈기에 의한 심층포기 호기조 MLSS (Mixed Liquor Suspended Solid) 침전성 향상 방안 연구)

  • Jisoo Han;Jeseung Lee;Byonghi Lee
    • Journal of Korean Society of Water and Wastewater
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    • v.38 no.3
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    • pp.165-175
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    • 2024
  • The dissolved air at the bottom layer of the deep aeration tank transforms into fine gas bubbles within the MLSS (Mixed Liquor Suspended Solid) floc when exposed to the atmosphere. MLSS floc flotation occurs when MLSS from the deep aeration tank enters the secondary clarifier for solid-liquid separation, as dissolved air becomes fine air within the MLSS floc. The floated MLSS floc causes a high SS (Suspended Solid) concentration in the secondary effluent. The fine air bubbles within the MLSS floc must be removed to achieve stable sedimentation in the secondary clarifier. Fine bubbles within the MLSS floc can be removed by air sparging. The settleability of MLSS was measured by sludge volume indexes (SVIs) after air sparging MLSS taken at the end of the deep aeration tank. MLSS settling tests were performed at MLSS heights of 200, 300, 400, and 500 mm, and compressed air was fed at the bottom of the settling column with air flow rates of 100, 300, and 500 ml/min at each MLSS height, respectively. Also, at each height and air flow rate, air was sparged for 3, 5, and 7 minutes, respectively. SVI was determined for each height, air flow rate, and sparging time, respectively. Experimental results showed that a 300 mm MLSS height, 300 ml/min air flow rate, and 3 minutes of sparging time were the least conditions to achieve less than 120 ml/g of SVI, which was the criterion for good MLSS settling in the secondary clarifier.

Solubility of Hydrogen Sulfide and Methane in Ionic Liquids: 1-Ethy-3-methylimidazolium Trifluoromethanesulfonate and 1-Butyl-1-methylpyrrolidinium Trifluoromethanesulfonate (1-Ethyl-3-methylimidazolium trifluoromethanesulfonate와 1-Butyl-1-methylpyrrolidinium trifluoromethanesulfonate 이온성 액체에 대한 황화수소와 메탄의 용해도)

  • Lee, Byung-Chul
    • Korean Chemical Engineering Research
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    • v.54 no.2
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    • pp.213-222
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    • 2016
  • Solubility data of hydrogen sulfide ($H_2S$) and methane ($CH_4$) in two kinds of ionic liquids with the same anion: 1-ethyl-3-methylimidazolium trifluoromethanesulfonate ([emim][TfO]) and 1-butyl-1-methylpyrrolidinium trifluoromethanesulfonate ([bmpyr][TfO]) are presented at pressures up to about 30 MPa and at temperatures between 303 K and 343 K. The gas solubilities in ionic liquids were determined by measuring the bubble point pressures of the gas + ionic liquid mixtures with various compositions at different temperatures using a high-pressure equilibrium apparatus equipped with a variable-volume view cell. The $H_2S$ solubilities in ionic liquid increased with the increase of pressure and decreased with the increase of temperature. On the other hand, the $CH_4$ solubilities in ionic liquid increased significantly with the increase of pressure, but there was little effect of temperature on the $CH_4$ solubility. For the ionic liquds [emim][TfO] and [bmpyr][TfO] with the same anion, the solubility of $H_2S$ as a molality basis was substantially similar, regardless of the temperature and pressure conditions as a molar concentration basis. Comparing the solubilities of $H_2S$ and $CH_4$ in the ionic liquid [emim][TfO], the solubilities of $H_2S$ were much greater than those of $CH_4$. For the same type of ionic liquid, the solubility data of $H_2S$ and $CH_4$ obtained in this study were compared to the solubility data of $CO_2$ from the literature. When compared at the same pressure and temperature conditions, the $CO_2$ solubility was in between the solubility of $H_2S$ and $CH_4$.