• 제목/요약/키워드: Boiler heat exchanger

검색결과 90건 처리시간 0.022초

보일러용 裸管 및 리브붙이管 의 熱傳達 特性 에 관한 硏究 (A Study on Heat Trasfer Characteristics of Smooth and Ribbed Tubes for Boiler)

  • 김종보;한승탁
    • 대한기계학회논문집
    • /
    • 제9권6호
    • /
    • pp.699-705
    • /
    • 1985
  • 본 논문에서는 자연 및 강제순환 모두를 실험 했으며 사용한 리브붙이 관은 관의 두께와 직경, 리브수, 리브 피치(Pitch), 높이 및 폭등을 사용 하려는 열교환기 나 보일러에 합당하도록 설계, 선정하면, 그 적용 범위는 매우 넓다고 생각돼 연구 검 토 하고자 한다.

Development of a Highly Efficient Boiler System Using a Diesel Engine

  • Lee, D.-H;Lee, D.-Y;Jo, M.-C;Cho, H.-N;Kim, Y.-S
    • Journal of Advanced Marine Engineering and Technology
    • /
    • 제28권2호
    • /
    • pp.367-375
    • /
    • 2004
  • We have developed a highly efficient boiler system using the 2,600cc Diesel engine. In this system, the co-generation concept is utilized in that the electric power is produced by the generator connected to the engine, and waste heat is recovered from both the exhaust gases and the engine itself by the shell-and-tube heat exchangers. The heat exchanger connected to the engine outlet is specially designed such that it not only recovers waste heat effectively from the exhaust gases, but significantly reduces an engine noise. It is found that the total efficiency(thermal efficiency plus electric power generation efficiency) of this system reaches maximum 96.3% which is about 15% higher than the typical Diesel engine boiler system currently being used worldwide.

가스보일러 코일형 열교환기의 열전달 특성에 관한 실험적 연구 (The Experimental Study on the Heat Transfer Characteristics)

  • 홍성혁;김영기;김일겸;김동춘;이창언;임장순
    • 태양에너지
    • /
    • 제17권4호
    • /
    • pp.57-66
    • /
    • 1997
  • The performance of gas-fired boilers were experimentally investigated. The heat exchanger used for the experiments consisted of circular tube with longitudinal fins for the gas side and a spiral coil for the water side. The burner was located at the top of the heat exchanger, and the burned gas flowed down to the exit. The experiments carried out for different water flow rates, the heat capacities of the boiler and the number of baffle. The thermal efficiency of the upward flow was higher than that of the downward flow of the water in the heat exchanger. As the boiler capacity increased, the thermal efficiency decreased. As the number of the baffles increase, the thermal efficiency increased and the increasing rate of the efficiency decreased. The gas-side overall heat transfer coefficient was independent of the flow rate of the water. The effect of the number of the baffles on the heat transfer coefficient was greater than that of the boiler capacity.

  • PDF

콘덴싱 가스보일러 잠열교환기의 이너 그루브 튜브 열유동 해석 (Heat Flow Analysis of Inner Groove Tube for Latent Heat Exchanger in Condensing Gas Boiler)

  • 용경중;임병철;박상흡
    • 한국산학기술학회논문지
    • /
    • 제15권7호
    • /
    • pp.4052-4056
    • /
    • 2014
  • 현재 가정용 콘덴싱 가스보일러의 사용을 의무화 하고 있는 추세이며, CO나 NOx와 같은 오염 물질의 배출이 적은 친환경 보일러 사용을 적극 추천하고 있다. 따라서 본 논문에서는 효율을 증가시키기 위하여 가정용 콘덴싱 가스보일러에 사용되는 2차열교환기인 잠열교환기의 튜브(관) 내부에 이너 그루브 형상을 추가 하여 열유동에 대한 해석을 실시하였다. 이너 그루브 형상이 추가됨에 따라서 전열면적은 약 20% 증가하였으며, 이에 따라 열전달량이 증가하는 것을 알 수 있었고, 이를 3차원 수치해석을 이용하여 확인하였다. 또한 이너 그루브 형상을 추가했을 경우 이너 그루브 형상이 없는 잠열교환기 보다 출구 온도가 약 $1^{\circ}C$ 증가하였고, 이는 가정용 콘덴싱 가스보일러의 효율증가에 상당한 도움이 될 것으로 판단된다.

다단 물유동층 열교환기에 의한 보일러 배가스의 폐열 회수 성능에 관한 연구 (A Study on the Heat Recovery from Boiler Exhaust Gas with Multi-stage Water-fluidized-bed Heat Exchanger)

  • 김대기;박상일;김한덕
    • 대한기계학회논문집B
    • /
    • 제25권12호
    • /
    • pp.1776-1783
    • /
    • 2001
  • Heat recovery from boiler exhaust gas with multi-stage water-fluidized-bed heat exchanger is analyzed in this study. The recovered energy here is not only sensible heat but also latent heat contained in the exhaust gas. In this system direct contact heat transfer occurs while exhaust gas passes through water bed and the thermal energy recovered this way is again delivered to the water circulating through heat exchanging pipes within the bed. Thus the thermal energy of exhaust gas can be recovered as a clean hot water. A computer program developed in this study can predict the heat transfer performance of the system. The results of experiments performed in this study agree well with the calculated ones. The heat and mass transfer coefficients can be fecund through these experiments. The performance increases as the number of stage increases. However at large number of stages the increasing rate becomes very low.

왕겨 연소기(燃燒機)를 이용(利用)한 온수(溫水)보일러 시스템 개발(開發) (I) -실험적(實驗的) 연구(硏究)- (Development of a Hot Water Boiler System with a Rice Hull Furnace)

  • 이용국;박승제;백풍기;노상하
    • Journal of Biosystems Engineering
    • /
    • 제12권4호
    • /
    • pp.31-43
    • /
    • 1987
  • This study was performed to develop a hot water boiler system with small scale automatic rice hull furnace for the multi-purpose use in the farm. For the experiment a prototype hot water boiler system with rice hull furnace was fabricated, which was equipped with automatic hull feeder, igniter and ash removal device. Optimum operational conditions of the prototype: system were analyzed. The results arc summarized as follows. 1. The temperature measured right above the burning surface should be higher than $500^{\circ}C$ combustion. 2. The top zone of the combustion chamber was the most suitable location of the thermocouple to pick up the control temperature for the automatic operation of the rice hull furnace. 3. The content of carbon monoxide in the flue gas was increased with the filling height of burning material but it was less than 0.3 percent in volume in this experiment. When the filling height was expressed as the ratio of rice hull feed rate to the volume of the combustion chamber above the burning surface, the optimum ratio was about $150kg/m^3-h$. 4. The combustion efficiency of the prototype was higher than 95 percent when the feed rate was 1.1 to 2.3 kg/h and moisture content of rice hull was 22.4 percent (w.b.) or less. 5. It was estimated that the optimum operational conditions of the system were 1.3 to 2.0 kg/h in feed rate, 70 to 100 percent in excess air and 500 to $510^{\circ}C$ in control temperature. 6. The efficiency of coil heal exchanger increased with a decrease in feed rate of rice hull. When the rice hull feed rates were 1.1, 1.7 and 2.3 kg/h, the efficiencies of coil heat exchanger were about 34, 30 and 25 percent and heat transfer rates were 5.7, 7.6 and 8.8 MJ/h, respectively. When the flat plate heat exchanger was used in addition to the coil heat exchanger, the efficiency of the heat exchanger system increased to 48 percent.

  • PDF

향온시설물에 대한 현열 및 잠열 에너지 회수시스템의 성능해석 (Performance Analysis of Sensible and Latent Energy Recovery System for Thermally Controlled Facilities)

  • 박병규;김무근;김근오
    • 설비공학논문집
    • /
    • 제12권12호
    • /
    • pp.1057-1065
    • /
    • 2000
  • A sizing of sensible and latent energy recovery system with condensing heat exchanger is important to the design of a thermally controlled facilities. The transient system simulation program TRNSYS 14.2/IISiBat has been used to evaluate the energy consumptions of a thermally controlled facilities which consist of boiler, chiller and condensing heat exchanger, The boiler and chiller are selected based on the annual peak loads and controlled to maintain the setting temperature of $14~17^{\circ}C$. Simulation shows that the amount of sensible and latent energy recovered by heat exchanger is almost 20% of total heating load.

  • PDF

직접접촉식 열교환기내에서 물과 배기가스의 직접접촉에 의한 열 및 물질전달 (Heat and Mass Transfer between Hot Waste Gas and Cold Water in a Direct Contact Heat Exchanger)

  • 이금배
    • 대한기계학회논문집
    • /
    • 제16권6호
    • /
    • pp.1171-1178
    • /
    • 1992
  • 본 연구에서는 직접접촉식 열교환기를 이용한 실험을 통하여 열교환기 설계에 가장 중요한 열교환기 단위 체적당 총괄 열전달 계수를 시스템의 작동조건에 따라 구 하여 실제 설계자료로 이용하는 데 그 목적이 있다.

열교환기용 고정형 튜브시트의 설계프로그램 개발 (Development of Design-Program of Fixed Type Tube-Sheet for Heat Exchanger)

  • 공제석;이경진;한정영;조종래;배원병
    • 소성∙가공
    • /
    • 제15권3호
    • /
    • pp.206-212
    • /
    • 2006
  • Design programs of tube-sheet for heat exchanger based on the related engineering society codes have been widely used. But it is not easy fer beginners to use the design programs. So we need to develop an easy program for design of tube-sheet for heat exchanger. This paper describes a developed design-program of tube-sheet fur heat exchanger. The developed program was coded on boiler theory and pressure vessel codes, provided by TEMA(Tubular Exchanger Manufactures Association) and ASME(American Society of Mechanical Engineers). Visual Basic, which is convenient for beginners to deal with, was used in the programming. Also a finite element analysis of tube-sheet for heat exchanger was carried to verify this developed program by using a commercial software, ANSYS. In the finite element analysis, tube and tube-sheet of heat exchanger were substituted by solid plate having equivalent properties for convenience of calculation. The thickness of tube-sheet obtained by the developed design-program was in good agreement with that of tube-sheet by FEA.

공장폐열(工場廢熱) 회수장치(回收裝置)에 관한 연구(硏究) -U자형(字型) 다관식(多管式) 열교환기(熱交換機)의 성능(性能)에 관하여- (Study on the Exhaust Heat Recovery Equipment in a Factory - On the Performance of a U-shape Multitube Heat Exchanger -)

  • 김영복;송현갑
    • Journal of Biosystems Engineering
    • /
    • 제8권2호
    • /
    • pp.49-61
    • /
    • 1983
  • U shape multitube heat exchanger was equipped in the flue to recover the exhaust heat from the boiler system. The fluids of the exhaust heat recovery equipment were the flue gas as the hot fluid, and the water as the cold fluid. The flow geometry of the fluids was cross flow - two pass, the hot fluid being mixed and the cold fluid unmixed. The results of the theoretical and the experimental analysis and the economic evaluation are summarized as follows. 1) The heat exchanger effectiveness and the temperature efficiency of the hot fluid were about 35% when the fuel consumption rate was 140 - 150 L/15min. The temperature efficiency for the cold fluid ranged from 3.0% to 4.5%. The insulation efficiency ranged from 85% to 98%, which was better than the KS air preheater insulation efficiency of 90%. 2) The relationship between the fuel consumption rate, F, and the outlet temperature, $T_{h2}$, of the flue gas from the heat exchanger was $T_{h2}$ = 0.927F + 110. In order to prevent the low temperature corrosion from the coagulation of $SO_3$, it is necessary to maintain the fuel consumption rate above 82 L/15min. 3) The ratio of the exhaust heat from the boiler system to the total energy consumption was about 14.5%. With the installation of the exhaust heat recovery equipment, the energy recovery ratio to the exhaust heat was about 25%. Accordingly, about 3.6% of the total fuel consumption was estimated to be saved. 4) Economic analysis indicated that the installation of the exhaust heat recovery equipment was feasible to save the energy, because the capital reocvery period was only 10 months when the fuel consumption rate was 80 L/15min. 4 months when it was 160 L/15min. 5) Based on the theoretical and the experimental analysis, it was estimated to save the energy of about 18 million Won per year, if four heat exchangers are installed in a factory. 6) A further study is recommended to identify the relationship among the flow rate of the exhaust gas, the size of the heat exchanger and the capacity of the air preheater. For a maximum heat recovery from the exhaust gas an automatic control system is required to control the flow rate of the cold fluid depending on the boiler load.

  • PDF