• Title/Summary/Keyword: Bearing preload

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Abnormal High-Temperature Behavior Troubleshooting of Process Compressor Tilting Pad Journal Bearing (프로세스 압축기 틸팅패드 저널베어링의 비정상 고온거동 트러블슈팅)

  • Lee, An Sung;Lee, Woonsil;Choi, Dong-Hoon
    • Tribology and Lubricants
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    • v.33 no.2
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    • pp.37-44
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    • 2017
  • A DE-side LBP tilting pad journal bearing of a 1-stage overhung heat-pump compressor in a propylene process exhibited abnormal high-temperature behavior. Its temperature had been relatively high at $78^{\circ}C$ from the beginning of operation. In 2014, after three years of operation, it increased suddenly and reached $103^{\circ}C$. Installing a varnish removal equipment and others managed to stabilize the temperature at $95^{\circ}C$. We undertook a troubleshooting approach for reviewing the comprehensive status and integrity of the temperature design of the bearing. We performed lubrication and heat-balance analysis, based on the design engineering data and documents supplied by the OEM. For the base design data of DE-side TPJB, evaluating the effects of key design variables on bearing metal temperature showed that firstly, increasing the bearing clearance and supply oil flow-rate, and next, changing the oil type, and finally, increasing the machined pad clearance and offset, are more effective in reducing the bearing metal temperature. Furthermore, a clarification meeting with the OEM revealed that an incorrect decision had been made to decrease the bearing clearance to eliminate the SSV harshness issue, while not maintaining a sufficient oil flow-rate. We conducted a detailed retrofit design analysis, wherein we increased the oil flow-rate and bearing clearance by decreasing the preload. We predicted that the bearing temperature would decrease to $63^{\circ}C$ from $75.7^{\circ}C$ even at the rerate condition. Finally, after installing and operating a retrofit replacement bearing in 2015, the bearing temperature stabilized at a low temperature of $65^{\circ}C$. Currently (January. 2017), two year later, the bearing metal temperature remains at $65^{\circ}C$. Therefore, we can conclude that the abnormal high-temperature behavior of the bearing has been resolved completely.

Vibration Control of Condensate Motors in Nuclear Powerplant By Bearing Redesign (베어링 재설계에 의한 원전 COP motor의 진동 제어)

  • Lim, Do-Hyeong;Kim, Won-Hyun;Lee, Jong-Moon;Lee, Soo-Mok
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2008.11a
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    • pp.264-269
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    • 2008
  • This paper presents the summary of control of abnormal vibration found in the COP motors of a nuclear power plant. All six identical units of COP pump-motor assemblies showed unstable vibration pattern of which one or two showed higher vibration enough to exceed the allowable level from the installation stage. Many trials of test, measurement, overhaul and replacement had been repeated to investigate and solve the problem but only to reach unsatisfactory settlement. Recently several times of site tests are made and followed by significant diagnostic actions in which the authors group participated. It was found that the coupled shafting system of motor and pump is in close resonance with the $1^{st}$ shaft rotating speed. Redesign of topside motor bearing clearance is made to increase bearing stiffness and hence to avoid the resonance which consequently led to reduce the troubled vibration to allowable and stable status.

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Analysis of the Motion Errors in Linear Motion Guide (직선베어링 안내면의 운동오차 해석)

  • Kim, Kyung-Ho;Park, Chun-Hong;Lee, Hu-Sang;Kim, Seung-Woo
    • Journal of the Korean Society for Precision Engineering
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    • v.19 no.5
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    • pp.139-148
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    • 2002
  • Motion errors of linear motion guideway are analyzed theoretically in this paper. For the analysis, an new algorithm predicting motion errors of bearing and guideway is proposed using the Hertz's elastic deformation theory. Accuracy averaging effect can be calculated quantitatively by analyzing relationship between motion errors of guideway and spatial frequency of rail form error. Influences of design parameters on the motion errors including the number of balls, preload, ball diameter, bearing length and the number of bearings are analyzed. As it is difficult to measure the rail form error, experimental results are compared with results analyzed by the equivalent analysis method which evaluate the motion errors of guideway using the measured errors of bearing. From the experimental results, it is confirmed that the proposed analysis method it effective lo analyze the motion errors of linear motion bearing and guideway.

Design Analysis for Enhancing Rotordynamic Stability of Process High-Speed Light weight Centrifugal Compressor - Part II: Improvements to Rotordynamic Stability (프로세스 고속 경량 원심 압축기의 로터다이나믹 안정성 강화를 위한 설계해석 - Part II: 로터다이나믹 안정성 개선)

  • Lee, An Sung
    • Tribology and Lubricants
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    • v.30 no.1
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    • pp.9-14
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    • 2014
  • In this Part II study, rotordynamic stability analyses were carried out to confirm improvements to the stability of a process high-speed lightweight centrifugal compressor, depending on the effects of tilting pad journal bearing designs. The bearing design variables considered were the clearances, LBPs, LOPs, and preloads. The results showed that the rotordynamic stability of the subject compressor rotor-bearing system improves exactly in accordance with the effects of the bearing design variables, which were determined in the preceding Part I study, owing to reduced bearing stiffnesses. Specifically, it was confirmed that the stability of the rotor system can be greatly improved by increasing both the machined and assembled bearing clearances, but there were no stability improvements by simply changing from an LBP to an LOP design. In addition, it was confirmed that for given fixed machined bearing clearances, the stability can be additionally improved by decreasing the preloads, i.e., by increasing the assembled clearances. In conclusion, it may be necessary to improve the designs of the original tilting pad bearings to obtain a sufficient margin of rotordynamic stability against a possible aerodynamic cross-coupled stiffness in a process high-speed centrifugal compressor. Thus, increasing the machined and assembled bearing clearances and decreasing the preload could be effective solutions.

Perturbed Finite Element Analysis of Fold Bifurcations in Load/unload Bard Disk Drive Systems (Load/Unload 하드디스크 드라이브 시스템에의 Fold Bifurcations의 교란 유한요소 해석)

  • Hwang Pyung;Khan Polina V.
    • 정보저장시스템학회:학술대회논문집
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    • 2005.10a
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    • pp.177-178
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    • 2005
  • The load/unload behavior of the hard disk drive slider is studied in terms of the air bearing static characteristics. The numerical continuation methods are applied to calculate suspension force - equilibrium position curve. The critical preloads of the femto size slider are analyzed. The hi-stability conditions are depicted on the skew angle - preload diagram. The perturbation method is used to check the stability of the solution branches.

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Simulation of Run-out caused by Imperfection of Ball Bearing for High-speed Spindle Units

  • Zverev Igor Aexeevich;Eun In-Ung;Chung Won-Jee;Lee Choon-Man
    • International Journal of Precision Engineering and Manufacturing
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    • v.7 no.3
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    • pp.3-7
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    • 2006
  • For the purpose to improve and to automate designing of high-speed spindle units (SU's), we have developed the mathematical models and software to estimate SU performance characteristics, including the run-out of spindles running on ball bearings. In order to understand better the mechanics of high-speed SUs, the dynamic interaction of ball bearings and SU, and the influence of the bearing imperfections and SU's operational conditions on the run-out, we have carried out computer simulation and experimental studies. Through the study of SU's, we have found out that run-out of SU can vary drastically with variation of rpm. The influences of rotation speed and of accuracy parameters of bearings on the SU accuracy have the greatest importance. The influence of bearing preload has a secondary importance. Comparison of the results of these studies has demonstrated adequacy of the models and software developed to the real SU's.

On the Bearing-to-Bearing Variability in Experimentally Identified Structural Stiffnesses and Loss Factors of Bump-Type Foil Thrust Bearings under Static Loads (범프 타입 포일 스러스트 베어링의 정하중 구조 강성 및 손실 계수 차이에 관한 실험적 연구)

  • Lee, Sungjin;Ryu, Keun;Jeong, Jinhee;Ryu, Solji
    • Tribology and Lubricants
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    • v.36 no.6
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    • pp.332-341
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    • 2020
  • High-speed turbomachinery implements gas foil bearings (GFBs) due to their distinctive advantages, such as high efficiency, lesser part count, and lower weight. This paper provides the test results of the static structural stiffnesses and loss factors of bump-type foil thrust bearings with increasing preload and bearing deflection. The focus of the current work is to experimentally quantify variability in structural stiffnesses and loss factors among the four test thrust bearings with identical design values and material of the bump and top foil geometries using the same (open-source) fabrication method. A simple test setup, using a rigidly mounted non-rotating shaft and thrust disk, measures the bearing bump deflections with increasing static loads on the test bearing. The inner and outer diameters of the test bearings are 41 mm and 81 mm, respectively. The loss factor, best-representing energy dissipation in the test bearings, is estimated from the area inside the local hysteresis loop of the load versus the bearing deflection curve. The measurements show that structural stiffnesses and loss factors of the test bearings significantly rely on applied preloads and bearing deflections. Local structural stiffnesses of the test bearings increase with applied preloads but decrease with bearing deflections. Changes of loss factors are less sensitive to applied preloads and bearing deflections compared to those of structural stiffnesses. Up to 35% variability in static load structural stiffnesses is found between bearings, while up to 30% variability in loss factors is found between bearings.

A Study on the Preload and Arrangement of Combined bearing on Feed Drive system (이송계에서 베어링 조합 배열과 예압량에 관한 연구)

  • 홍성오
    • Proceedings of the Korean Society of Machine Tool Engineers Conference
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    • 1999.10a
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    • pp.440-445
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    • 1999
  • One of the important technical issues is how to decrease thermal expansion of ballscrew in proportion to the increase of machining speed. When measuring force of stretch of ballscrew, since not only actual expansion and the value of bending have to be considered, it's impossible to definite the exact value of expansion. In addition, support bearings of ballscrew gain considerable force in axial direction. It also generates thermal expansion on the ballscrew, and deteriorates the bearings. In conclusion, it's impossible to give the pretension enough to absorb the all elongation due to thermal expansion generated during machine running. If gave, bed, column and saddle are all bent to change machine accuracy, and the pretension of support bearing of ballscrew in machine tool.

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Load-transferring mechanism and evaluation theory of bolt with single and double nut fasteners

  • Qiyu Li;Dachang Zhang;Hao Xu;Yibi Li;Weiqun Chen;Kaixuan Zhang
    • Structural Engineering and Mechanics
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    • v.86 no.2
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    • pp.261-276
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    • 2023
  • The use of the ordinary double nut (i.e., ODN) composed of a master nut (i.e., M-nut) and a slave nut (i.e., S-nut) is a highly efficient method to prevent bolts loosening. A novel double nut (i.e., FODN) composed of a master nut (i.e., M-nut) and flat slave nut (i.e., FS-nut) is proposed to save raw materials. The bolt fastening tests with single nut, ODN and FODN are performed to investigate the preload and counterbalance forces. Corresponding finite element analysis (FEA) models are established and validated by comparing the preload with the experimental results. The load-bearing capacity, the extrusion effect, and the contact stress of each engaged thread for ODN and FODN are observed by FEA. The experimental and simulated results revealed that the bolt fastening with double-nut has different load-transferring mechanisms from single-nut. Nevertheless, for double-nut/bolt assemblies, the FS-nut can provide load transfer that is like that of the S-nut, and the FODN is a reasonable and reliable fastening method. Furthermore, based on the theory of Yamamoto, a formula considering the extrusion effect is proposed to calculate the preload distribution of the double-nut, which is applicable to varying thicknesses of slave-nuts in double-nut/bolt assemblies.