• 제목/요약/키워드: Agricultural Heater

검색결과 89건 처리시간 0.024초

온풍난방기의 열효율 증대를 위한 열교환기 구조개선 (Mechanism Improvement of the Heat Exchanger for the Thermal Efficiency Increase of Hot Air Heater)

  • 강금춘;강연구;유영선;김영중;이시영;백이
    • Journal of Biosystems Engineering
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    • 제34권5호
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    • pp.363-370
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    • 2009
  • Hot air heater with light oil combustion is used as the most common heater for greenhouse heating in the winter season. Hot air heaters of 256,246 units have been supplied as main greenhouse heating equipment until 2008 and greenhouse heating cost has reached to 620 billions won in Korea. In order to improve the thermal efficiency of the hot air heater and to reduce the expenses for greenhouse heating, prototype hot air heater was manufactured and tested in this experiment. The heat exchanger of tested prototype hot air heater was circular and hexagonal pipe type and inline and stagger arrangement type. Capacity of the heating was 43,062 kJ/h and total heat transfer area of the heat exchanger was $10.728\;m^2$. According to the performance test, it could supply heat of 38,240 to 35,100 kJ/h depending on the fan motor speed of 1,740~1,220 rpm, respectively. Thermal efficiency of hot air heater was 87.0% to 80.8% in the same conditions. As a result, thermal efficiency of hot air heater with hexagonal pipe-stagger arrangement heat exchanger developed in this study was higher 10.2% than that of conventional hot air heater and heating energy saving rate of 14.3% increased.

2단 응축 히트펌프 온수시스템의 사이클 해석 및 성능분석 (Performance of Heat Pump Water Heater with Dual Condenser)

  • 유영선;김영중;강금춘;백이;윤진하;강연구;이형모
    • Journal of Biosystems Engineering
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    • 제31권5호
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    • pp.423-429
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    • 2006
  • The heat pump water heater developed in this research consisted of one evaporator, one compressor, 1st condenser, 2nd condenser, one expansion valve, one water tank, one recirculation circuit and etc. The performance of heat pump water heater was tested and analyzed. The quantities of output water changed linearly from 2380 to $660{\ell}/h$, and the output water temperature changed curvedly from 29.9 to $44.5^{\circ}C$ when the opening rate of recirculation valve changed from 0 to 100%. The COP of heat pump water heater increased from 3.0 to 3.8 when the quantities of output water changed from 660 to $2380{\ell}/h$. When the temperature distributions of water tank were measured during 50 minutes after turning on the heat pump, the temperature stratification by the level appeared apparently. When the inlet water temperature changed from 30 to$50^{\circ}C$, the output energy of heat pump hardly changed. The surface area of double pipe heat exchanger changed from 0.429 to $6.254m^2$ when the compressor capacity increased from 1.0 to 50.0 PS.

Growth effects of novel heating system using heater-installed rearing tray on silkworm, Bombyx mori

  • Jeong, Chan Young;Kim, Kee Young;Kim, Nam-Suk;Kang, Sang Kuk;Park, Jong Woo;Cha, Ik Seob;Kim, Seong-Wan
    • International Journal of Industrial Entomology and Biomaterials
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    • 제45권1호
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    • pp.22-28
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    • 2022
  • Silkworms are very sensitive to changes in temperature and humidity, and unless it is a suitable temperature and humidity to grow, the productivity and quality of silkworms are greatly reduced. Therefore, it is very important to manage temperature and humidity for silkworm feeding facilities. In particular, it is essential to install heating facilities in Asian countries with distinct seasonal changes. During the feeding period, many farms manage the temperature and humidity of feeding facilities by installing and using electric heaters inside the facilities. However, it is very difficult to manage the room temperature stably by the heaters. In addition, unlike the temperature inside the facility, silkworms could undergo severe temperature changes as the inside of the rearing tray could not be warm enough. In this study, in order to improve the previous heating method, the new rearing method that directly heats the bottom of the rearing tray was developed. Compared to the previous room-heating system, the novel heater-installed tray (HIT) system significantly reduced the change in temperature during the experimental period. In addition, the number of days of silkworm growth up to harvest was shortened, which was effective in growth performance, and it was also found that silkworms grew more uniformly in HIT system than in previous system. Moreover, as the heater tubes were installed directly under the rearing tray, it quickly dried mulberry leaves and silkworm feces after feeding, and as a result, the environment in the tray was greatly improved with decrease the labor of breeder. In conclusion, these results suggest that the heater-installed rearing tray method greatly improves silkworm quality, increases weight of silkworms, and final profits compared to the previous room heating system with electric heaters.

히트파이프를 활용한 농업용 고효율난방기 및 스마트 제어시스템 (High-efficiency Agricultural Heater and Smart Control System Utilizing Heat Pipe)

  • 김응곤;임창균
    • 한국전자통신학회논문지
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    • 제12권6호
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    • pp.1151-1158
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    • 2017
  • 히트파이프 일체형 고효율 난방기는 겨울철 시설원예 내 작물생육에 필수인 난방장치와 배기열 회수기를 일체화하여 배기열이 외부로 배출되기 전 미사용 에너지를 재이용하는 장치이다. 시설원예, 유리온실 등 점검을 통해 우리나라 농업용 난방기의 문제점을 파악하였고, 개선방향을 찾아 시설원예 및 하우스에 맞는 최적화된 농업용 고효율난방기 및 스마트 제어시스템을 제안하였다.

EXHAUST GAS HEAT RECOVERY SYSTEM FOR PLANT BED HEATING IN GREENHOUSE PRODUCTION

  • Kim, Y.J.;Ryou, Y.S.;Rhee, K.J.;Kang, G.C.
    • 한국농업기계학회:학술대회논문집
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    • 한국농업기계학회 2000년도 THE THIRD INTERNATIONAL CONFERENCE ON AGRICULTURAL MACHINERY ENGINEERING. V.III
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    • pp.639-646
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    • 2000
  • Hot air heater with light oil combustion is the most common heater for greenhouse heating in the winter season in Korea. However, since the heat efficiency of the heater is about 80%, considerable unused heat in the form of exhaust gas heat discharges to atmosphere. In order to capture this exhaust gas heat a heat recovery system for plant bed heating in the greenhouse was built and tested in the hot air heating system of greenhouse. The system consists of a heat exchanger made of copper pipes, ${\phi}\;12.7{\times}0.7t$ located inside the rectangular column of $330{\times}330{\times}900mm$, a water circulation pump, circulation plastic pipe and a water tame The total heat exchanger area is $1.5m^2$, calculated considering the heat exchange amount between flue gas and water circulated in the copper pipes. The system was attached to the exhaust gas path. The heat recovery system was designed as to even recapture the latent heat of flue gas when exposing to low temperature water in the heat exchanger. According to performance test it can recover 45,200 to 51,000kJ/hr depending on the water circulation rates of 330 to $690{\ell}$/hr from the waste heat discharged. The exhaust gas temperature left from the heat exchanger dropped to $100^{circ}C$ from $270^{circ}C$ by the heat exchange between the water and the flue gas, while water gained the difference and temperature increased to $38^{circ}C$ from $21^{circ}C$ at the water flow rate of $690{\ell}$/hr. And, the condensed water amount varies from 16 to $43m{\ell}$ at the same water circulation rates. This condensing heat recovery system can reduce boiler fuel consumption amount in a day by 34% according to the feasibility study of the actual mimitomato greenhouse. No combustion load was observed in the hot air heater.

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전기히터식 및 지열원 히트펌프식 농산물 열풍건조기의 에너지 성능 비교 (Energy Performance Comparison of Electric Heater and Geothermal Source Heat Pump type Agricultural Hot Air Dryers)

  • 양원석;김영일;박승태
    • 한국지열·수열에너지학회논문집
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    • 제14권4호
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    • pp.7-12
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    • 2018
  • Energy performance of electric heater and geothermal source heat pump type hot air dryers are compared in this study. For set temperatures of $30^{\circ}C$, $35^{\circ}C$ and $40^{\circ}C$, radish is dried from initial mass 60 kg until it gets 5 kg, where the difference equals the amount of water removed. As set temperature is increased, drying time is shortened for both electric heater and heat pump types, however energy efficiency is decreased due to increasing electricity consumption. Moisture extraction rate(MER) of electric heater is 2.58~2.84 kg/h, and for heat pump type 2.56~2.71 kg/h, showing little difference between the two types. Specific moisture extraction rate (SMER) of electric heater is 0.94~0.96 kg/kWh, and for heat pump type 1.72~2.21 kg/kWh. SMER of heat pump type is greater by 0.78~1.25 kg/kWh than the electric heater hot air dryer, which is 1.8~2.3 times better in terms of energy efficiency.

농업용 온풍난방기에서 동물성바이오디젤의 연소특성 (Characterizing Animal-fats Biodiesel as Heating Fuel for Agricultural Hot Air Heater)

  • 김영중;박석호;김충길;김영진
    • 한국신재생에너지학회:학술대회논문집
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    • 한국신재생에너지학회 2011년도 추계학술대회 초록집
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    • pp.115-115
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    • 2011
  • Biodiesel (BD) was made from animal-fats reacting with methanol and potassium hydroxide in the laboratory. The biodiesel made in the laboratory was sent to K-petro, the government agency, to inspect the quality of animal-fats biodiesel, of which generally the quality was acceptable for heating oil for agricultural hot air heater. Kinematic viscosity and calorific values of the biodiesels were measured. BD20(K), kerosene based biodiesel, showed 18cSt at $-20^{\circ}C$. It seems that BD100 can not be suitable for heating fuel under some temperature. As BD content increased calorific value decreased, up to 40,000J/g for 100% BD, while light oil calorific value was 45,567J/g, showing difference of 5,567J/g, about 12% difference. Several different fuels, BD20, BD50, BD100 and light oil, were prepared and tested for fuel combustion qualities for agricultural hot air heater and their combustion performances were compared and analyzed. Flame dimensions of biodiesels and light oil were almost same shape at the same combustion condition in the burner of the hot air heater. Generally $CO_2$ amounts of BDs are greater than light oil. But,the differences are so small that it is hard to tell there was significant difference existed between the BDs combustion and light oil.

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Fuel Qualities and Combustion Characteristics of Animal-Fats Biodiesel for Agricultural Hot Air Heaters

  • Kim, Youngjung;Park, Seokho;Kim, Youngjin;Kim, Chungkil
    • Journal of Biosystems Engineering
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    • 제37권5호
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    • pp.296-301
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    • 2012
  • Purpose: Combustion and fuel qualities of the animal-fats biodiesel as a heating fuel for agricultural hot air heater were studied. Methods: Biodiesel (BD) was made from animal-fats by reacting with methanol and potassium hydroxide in the laboratory. The biodiesel made in the laboratory was tested for fuel and combustion qualities. Results: The kinematic viscosity and the calorific values of the biodiesels were measured. Kerosene based biodiesel, BD20 (K) showed 18 cSt at $-20^{\circ}C$. It seemed that BD100 was not suitable for a heating fuel under some temperature. As BD content increased, the calorific value decreased up to 40,000 J/g for BD100, while the calorific value of light oil was 45,567 J/g showing difference of 5,567 J/g, about 12% difference. Several different fuels including BD20 (biodiesel 20% + light oil 80%), BD50 (biodiesel 50% + light oil 50%), BD100 (biodiesel 100%), and light oil were tested for fuel combustion qualities for agricultural hot air heater, and their combustion performances were compared and analyzed. Flame dimensions of biodiesels and light oils were almost the same shape at the same combustion condition. Generally, the $CO_2$ amounts of BDs were greater than light oil. However, in this study the differences were minor, so there was no significant difference existed between the BDs combustion and light oil. Conclusions: It seemed that quality was good for heating oil for agricultural hot air heater because of showing no barriers for continuous combustion and proper exhaust gas temperature and $CO_2$ amount discharged. But, for fuel fluidity for higher BD content fuel could be a detrimental problem in situations where the outdoor temperature is lowered. As BD content increased, calorific value decreased up to 40,000 J/g for BD100. Calorific value difference between BD20 and light oil was about 1,360 J/g.

히트파이프를 이용한 온풍난방기 배기열회수 시스템의 열회수 특성 (Heat Recovery Characteristics of the Exhaust Heat Recovery System with Heat Pipe Unit Attached to the Hot Air Heater in the Greenhouse)

  • 강금춘;김영중;유영선;백이;이건중
    • Journal of Biosystems Engineering
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    • 제26권5호
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    • pp.441-448
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    • 2001
  • Hot air heater with light oil combustion is used as the most common heater for greenhouse heating in the winter season. However, exhaust gas heat discharged to atmosphere through chimney reaches up to 10~20% of total heat capacity of the oil burred. In order to recover the heat of this exhaust gas and to use for greenhouse heating, the heat pipe type exhaust heat recovery system was manufactured and tested in this experiment. The system consisted of a heat exchanger made of heat pipes, ø15.88${\times}$600mm located in the rectangular box of 675(L)${\times}$425(W)${\times}$370(H)mm, an air suction fan and air ducts. The number of heat pipe was 60, calculated considering the heat exchange amount between exhaust gas and air and heat transfer capacity of a heat pipe. The working fluid of heat pipe was acetone because acetone is known for its excellent heat transfer capacity. The system was attached to the exhaust gas path. According to the performance test it could recover 53,809 to 74,613kJ/h depending on the inlet air temperature of 12 to -12˚at air flow rate of 1.100㎥/h. The temperature of the exhaust gas left the heat exchanger dropped to 100$^{\circ}C$ from 270$^{\circ}C$ after the heat exchange between the suction air and the exhaust gas.

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시설원예용 온풍난방기내의 온도분포에 관한 연구 (I) - 난방유 사용시 온도특성 - (Temperature Distributions inside a Space Heater for Greenhouse (I) - Temperature Characteristics with Heating Oil -)

  • 서정덕;김종진;최규성;신창식;노수영
    • Journal of Biosystems Engineering
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    • 제24권4호
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    • pp.335-342
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    • 1999
  • Air and flue gas temperature distributions in the space heater for greenhouse were measured to develop a thermal design technology for the space heater. Also, the characteristics of the fan supplying air to the space heater were investigated. The temperature of the flue gas inside the flue gas tube was linearly decreased as the lenght of than those of the flue gas with the oxygen concentration of 8.25% at the last exit of the second flue gas tube. Thus, the operating efficiency of the space heater could be increased with low air ratio decreased exhausting gas temperature and saved the energy consumption with decreased excess air flow. The temperature of the air supplied by fan was increased slowly around the first flue gas tube, meanwhile, increased sharply around the second flue gas tube due to large LMTD (Logarithmic Mean Temperature Difference) at the first flue gas tube than which of the second flue gas tube.

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