• Title/Summary/Keyword: Absorbing torque

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Drive-train Jerk Reduction Control for Parallel Hybrid Electric Vehicles (병렬형 하이브리드 전기자동차 구동계의 Jerk 저감 제어)

  • Park, Joon-Young;Sim, Hyun-Sung
    • Transactions of the Korean Society of Automotive Engineers
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    • v.19 no.1
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    • pp.17-24
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    • 2011
  • TMED(Transmission Mounted Electric Device) parallel hybrid configuration can realize EV(Electric Vehicle) mode by disengaging the clutch between an engine and a transmission-mounted motor to improve efficiencies of low load driving and regenerative braking. In the EV mode, however, jerk can be induced since there are insufficient damping elements in the drive-train. Though the jerk gives demoralizing influence upon driving comport, adding a physical damper is not applicable due to constraints of the layout. This study suggests the jerk reduction control, composed of active damping method and torque profiling method, to suppress the jerk without hardware modification. The former method creates a virtual damper by generating absorbing torque in the opposite direction of the oscillation. The latter method reduces impulse on the mated gear teeth of the drive-train by limiting the gradient of traction torque when the direction of the torque is reversed. To validate the effectiveness of the suggested strategy, a series of vehicle tests are carried out and it is observed that the amplitude of the oscillation can be reduced by up to 83%.

The study on the influences of vibration associated with cycling on the human body (자전거 주행 중 발생하는진동이 인체에 미치는 영향)

  • Chung, Kyung-Ryul;Hyeong, Joon-Ho;Kim, Sa-Yup
    • Proceedings of the Korean Society for Noise and Vibration Engineering Conference
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    • 2009.10a
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    • pp.643-646
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    • 2009
  • This study was conducted to simulate the influence of vibration associated with cycling on the body. In this simulation the human model that the riding on a bicycle which have suspension and non-suspension front forks was used. And to arouse impact two kind of bump, 50mm height of radical raised spot and 150mm height of slow raised spot, were used. The vertical displacement of head, the vertical acceleration of head and the torque of neck joint were analysed. The results say that the function of shock absorbing was grater when passing though a 50mm height of radical raised spot then a 150mm height of slow raised spot.

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Development of Flange Flexible Urethane-key Coupling (플랜지 플렉시블 우레탄카 커플링 개발)

  • Cho, Young-Tae;Lee, Ki-Yong;Lee, Choong-Ho
    • Journal of the Korean Society of Manufacturing Technology Engineers
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    • v.19 no.5
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    • pp.667-671
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    • 2010
  • The study was aimed at developing a power transmission coupling that is possible to transfer power without any trouble even if the two rotating shafts are making minute misalignment. The coupling that has been developed is Flange Flexible Urethane-key Coupling that connects two shafts by flanges with Urethane-key. A model coupling for use in transmitting power of 10hp was made and undergone performance evaluation and tests. Property and usefulness was proved through the test. The performance evaluation has demonstrated a property of $11.25Kgf{\cdot}m$ of allowable torque and 28.25hp of power at 1,80Orpm, which was found to be superior compared to the performance of similar couplings. Based on the performance test, study was made also for improving the shape of the Urethane-key and was successful to make the flange in smaller outside diameter. Further application test at site has proved that the product is easy to install and maintain, and has property of absorbing minute misalignment between two shafts and vibration caused there from.

The Study on Improvement about Structural Integrity of Main Landing Gear for Rotorcraft (회전익 항공기 구조건전성 향상을 위한 주륜착륙장치 결함 개선연구)

  • Jang, Min-Uk;Lee, Yoon-Woo;Seo, Young-Jin;Ji, Sang-Yong
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.20 no.10
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    • pp.459-467
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    • 2019
  • The landing gear is a component that requires a high degree of safety to protect the lives of rotary-wing aircraft and boarding personnel, absorbing the impact on transfer/landing and supporting the fuselage during taxiing and mooring on the ground. In particular, the wheel landing gear supporting the aircraft fuselage absorbs most of the shock from the ground through the shock absorber and tires. This ensures the safety of the pilot on board the aircraft and satisfies the operational capability of the soldiers between missions. During the operation of a rotary-wing aircraft, a number of piston pins, which are a component of the right main wheel landing gear, were found to be broken. Therefore, this study examined the root cause of the piston pin crack phenomenon found in the main wheel landing gear. For this purpose, various causes were identified from fracture surface analysis of a flight test. In particular, the possibility of cracking was analyzed based on the influence on the fastening torque with the drag beam component applied to the piston pin at the time of development. This ensures the fatigue life and structural integrity.