• Title/Summary/Keyword: 희박 예혼합 예증발

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Design of Venturi Dump Surface for Pre-filming Airblast Injector (예막 공기충돌형 분사기의 벤추리 덤프면 설계)

  • Shin, Dongsoo;Choi, Myunghwan;Radhakrishnan, Kanmaniraja;Koo, Jaye;Jung, Seungchai
    • Journal of the Korean Society of Propulsion Engineers
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    • v.22 no.4
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    • pp.44-54
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    • 2018
  • In a spray experiment using a venturi mounted on a lean premixed LPP injector, droplets appear to have non-uniform distributions. To solve this problem, the exit angle of the venturi was changed to form a dump surface on the nozzle neck. The dump surface improved the atomization performance and minimized droplet loss while forming recirculation zone in the venturi exit. In order to solve the non-uniform spray of the injector, the flow characteristics inside the venturi and SMD of the spray are compared. Finally, an optimum venturi shape is selected to minimize the spray loss and improve the spray performance.

The Combustion Characteristics at Primary Zone of Lean Premixed low NOx Combustor (저 NOx 희박연소기의 주연소영역에서의 연소특성 연구)

  • Lim, A.H.;Ahn, K.Y.;Kim, H.S.;Kim, Y.M.
    • Proceedings of the KSME Conference
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    • 2003.11a
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    • pp.314-319
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    • 2003
  • The concept of lean-premixed combustion in gas turbine combustor operation has become a standard in recent years as an effective means to meet stringent enviromental standards on NOx emissions. The combustion characteristics of 75 kW class lean premixed combustor were investigated at the conditions of high temperature and ambient pressure. The exit temperature and emissions of CO and NOx were measured at the center of exit plane. The high temperature air of $550K{\sim}650K$ was supplied through air preheater. As expected, experimental results indicate that NOx emission was increased and CO emission was decreased by increasing inlet air temperature. But CO emission measured at the center of exit plane was increased because of the non-uniform radial direction profiles. The Semi-Empirical Correlation method was applied to obtain the design point emissions of NOx and CO. Also the flame temperature, CO and NOx emissions were measured along the centerline of liner at 650K inlet air temperature to determine the position of dilution holes.

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