• Title/Summary/Keyword: 확공지압형 앵커 시스템

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Comparison Analysis of the Environmental Impact of VSL Anchors and RBanchors Using a Life-Cycle Assessment (LCA) (LCA를 이용한 확공지압형 앵커와 일반 앵커의 환경영향 특성 비교분석)

  • Ahn, Taebong;Lee, Jaewon;Min, Kyoungnam;Lee, Junggwan;Kwon, Yongkyu
    • Journal of the Korean Society for Railway
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    • v.18 no.6
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    • pp.558-566
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    • 2015
  • In this study, quantitative environmental impact assessments of the VSL anchor and RB(Reaming and Bearing) anchor systems were conducted after a life-cycle assessment (LCA). In addition, improvements which reduce the adverse environmental effects of the RB anchor system were confirmed through comparisons with results with a VSL anchor system. Both results showed that water ecotoxicity and global warming are the most important in environmental influences. To determine the effect of reducing the RB anchor system environment, the result was normalized for the environmental impact category. Most items appeared to have been improved with regard to the RB anchor system. The most significant improvement was a 77% decrease in POC levels(photochemical oxidant creation). Greenhouse gas emissions, related to global warming, were decreased by 44%. It is expected that these quantitative environmental impact assessment results will serve as the basis of an anchor system for civil engineering and environmental impact assessments.

Behavior Characteristics of Underreamed Ground Anchor through Field Test and Numerical Analysis (현장시험 및 수치해석을 통한 확공지압형 앵커의 거동특성)

  • Kim, Gyuiwoong;Ahn, Kwangkuk;Min, Kyongnam;Jung, Chanmuk
    • Journal of the Korean GEO-environmental Society
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    • v.14 no.8
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    • pp.37-44
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    • 2013
  • The superiority of bearing ground anchor system has been recognized for the stability and economical efficiency since 1950s in Japan, Europe and etc. The ground anchor introduced in Korea, however, has the structural problem that the tensile strength comes only from the ground frictional force caused by the expansion of the wedge body and it is impossible to evaluate the bearing resistance because the adhering method of the anchor body to hollow wall is not appropriate. In this study, the underreamed ground anchor system was developed so that the bearing pressure of ground anchor can exert as much as possible. And the in-situ tests were performed to evaluate the pullout behavior characteristics and to verify the decreasing effect of the bonded length. The pullout tests were performed with the non-grouted tension condition and grouted tension condition in order to identify the pull-out resistance of each conditions. In addition, it was compared with the results of friction anchor. Finally, the numerical analysis was fulfilled to verify the bearing effect at the bonded part through the detailed modeling by PLAXIS-2D, which is general finite element method analysis program.