• Title/Summary/Keyword: 항공정비결함

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A Study on Contributing Factors to Aircraft Maintenance Failure (항공정비결함에 기여하는 인적요인에 관한 연구)

  • Kim, Chun-Yong;Park, Heui-Kwan
    • Journal of the Korean Society for Aviation and Aeronautics
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    • v.25 no.3
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    • pp.81-88
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    • 2017
  • Aircraft maintenance failure doesn't only threaten flight safety but also causes significant economic losses such as flight delays, flight cancellations, air turn backs and diversion and so on. Therefore, the efforts should be made to detect the contributing factors that cause such maintenance failure and eliminate them. In this study, by analyzing factors contributing to system failure using the Maintenance Error Decision Aid (MEDA) model based on stochastic relations between the contribution factors, system failure and events, we will draw a improvement plan to aircraft maintenance defects.

A Study on the Improvement of the Domestic Maintenance Capability Development System of Military for Overseas Maintenance Items through the Case Study of Intermittent Failure of an Avionics (항전계통 간헐결함 사례 분석을 통한 군의 해외 정비품 국내정비능력 개발제도 개선방안 고찰)

  • Lee, Hoyong
    • Journal of the Korean Society for Aviation and Aeronautics
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    • v.26 no.2
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    • pp.68-75
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    • 2018
  • A flare from an Air Force fighter was abnormally dispensed during the landing. To determine the cause of the abnormal dispensing, fracture analysis, signal analysis and reproduction experiments based on physics of failures were performed. The primary cause of the failure was analyzed to be due to an intermittent fault of an internal circuit card in the AN/ALE-40 chaff/flare dispenser by a broken lid of a capacitor, and the root cause which had derived the primary cause was considered to be an improper handling during the domestic maintenance which were changed from the overseas maintenance due to the DMSMS problem. Therefore, the overall process of the maintenance capability development system was reviewed and alternative ways that considers maintenance error decision aid(MEDA) for system improvement were suggested to prevent further failures.

Design and Verification of Built In Test For KUH (한국형 기동헬기 자체진단 시험 설계 및 입증)

  • Kim, Sung-Woo;Lee, Byoung-Hwa;Chang, Won-Hong;Oh, Woo-Seop
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.40 no.7
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    • pp.623-628
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    • 2012
  • Mission Equipment Package(MEP) system is a collection of avionic components that are integrated to perform the mission of the Korean Utility Helicopter(KUH). Built In Test(BIT) reduces the need for skilled personnel and special test equipment, and reduces maintenance down-time of system. The increasing complexity of avionics equipments has resulted in an increased need to provide BIT functions. This paper describe the development and verification for the KUH MEP system BIT.

A Study on the Concept of a Ship Predictive Maintenance Model Reflection Ship Operation Characteristics (선박 운항 특성을 반영한 선박 예지 정비 모델 개념 제안)

  • Youn, Ik-Hyun;Park, Jinkyu;Oh, Jungmo
    • Journal of the Korean Society of Marine Environment & Safety
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    • v.27 no.1
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    • pp.53-59
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    • 2021
  • The marine transport industry generally applies new technologies later than other transport industries, such as airways and railways. Vessels require efficient operation, and their performance and lifespan depend on the level of maintenance and management. Many studies have shown that corrective maintenance (CM) and time-based maintenance (TBM) have restrictions with respect to enabling efficient maintenance of workload and cost to improve operational efficiency. Predictive maintenance (PdM) is an advanced technology that allows monitoring the condition and performance of a target machine to predict its time of failure and helps maintain the key machinery in optimal working conditions at all times. This study presents the development of a marine predictive maintenance (MPdM; maritime predictive maintenance) method based on applying PdM to the marine environment. The MPdM scheme is designed by considering the special environment of the marine transport industry and the extreme marine conditions. Further, results of the study elaborates upon the concept of MPdM and its necessity to advancing marine transportation in the future.

The Meaning of Extraordinary Circumstances under the Regulation No 261/2004 of the European Parliament and of the Council (EC 항공여객보상규칙상 특별한 사정의 의미와 판단기준 - 2008년 EU 사법재판소 C-549/07 (Friederike Wallentin-Hermann v Alitalia) 사건을 중심으로 -)

  • Kim, Young-Ju
    • The Korean Journal of Air & Space Law and Policy
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    • v.29 no.2
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    • pp.109-134
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    • 2014
  • Regulation (EC) No 261/2004 of the European Parliament and of the Council of 11 February 2004 establishing common rules on compensation of assistance to passengers in the event of denied boarding and of cancellation or long delay of flights (Regulation No 261/2004) provides extra protection to air passengers in circumstances of denied boarding, cancellation and long-delay. The Regulation intends to provide a high level of protection to air passengers by imposing obligations on air carriers and, at the same time, offering extensive rights to air passengers. If denied boarding, cancellation and long-delay are caused by reasons other than extraordinary circumstances, passengers are entitled for compensation under Article 7 of Regulation No 261/2004. In Wallentin-Hermann v Alitalia-Linee Aeree Italiane SpA(Case C-549/07, [2008] ECR I-11061), the Court did, however, emphasize that this does not mean that it is never possible for technical problems to constitute extraordinary circumstances. It cited specific examples of where: an aircraft manufacturer or competent authority revealed that there was a hidden manufacturing defect on an aircraft which impacts on safety; or damage was caused to an aircraft as a result of an act of sabotage or terrorism. Such events are not inherent in the normal exercise of the activity of the air carrier concerned and is beyond the actual control of that carrier on account of its nature or origin. One further point arising out of the court's decision is worth mentioning. It is not just necessary to satisfy the extraordinary circumstances test for the airline to be excused from paying compensation. It must also show that the circumstances could not have been avoided even if all reasonable measures had been taken. It is clear from the language of the Court's decision that this is a tough test to meet: the airline will have to establish that, even if it had deployed all its resources in terms of staff or equipment and the financial means at its disposal, it would clearly not have been able - unless it had made intolerable sacrifices in the light of the capacities of its undertaking at the relevant time - to prevent the extraordinary circumstances with which it was confronted from leading to the cancellation of the flight.

Fatigue Analysis to Determine the Repair Limit for the Damaged Fastener Hole of Aging Aircraft(P-3CK) (노후항공기(P-3CK) 패스너 홀 손상 수리 한계 설정을 위한 피로해석)

  • Kim, Young-Jin;Kim, Hyeung-Geun;Kim, Chang-Young;Chang, Joong-Jin;Lee, Mal-Young
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.41 no.12
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    • pp.959-966
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    • 2013
  • In this study, based on P-3CK project using aging aircraft without any design information, the structural assessments of fastener holes to repair the short edge distance defects are investigated. For this purpose, the nacelle longeron which has many defects is selected and then conservative stress is calculated by performing the static analysis of 1.5ED, 1.8ED, 2.0ED defects of longeron fastener holes. This result applies to TWIST standard load spectrum to generate flight load spectrum. Then the crack growth analysis is performed by using flight load spectrum. Through this, the validity of a repaired fastener hole is evaluated. Finally, the standard of repair and the period of maintenance for a defected fastener hole are established.

The Study on Improvement of Thermal Stress Breakage in Infrared Transmissive Glass for Aircraft Searchlight (항공기용 탐조등 적외선 투과 유리의 열응력 파손 현상 개선 연구)

  • Seo, Young-Jin;Jeong, Sang-Gyu
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.19 no.11
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    • pp.332-337
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    • 2018
  • Aircraft searchlights are used in search or rescue missions when performing night missions, and provide infrared light to keep operations in concealment. During aircraft operation, the infrared ray transmission filter glass for generating infrared rays can break, resulting in problems such as loss of concealment ability and maintenance. In this paper, we describe the procedure for testing the operating conditions of the searchlight when the defect occurs and finding the cause of the defect. We also summarize various methods to improve the cause and process of making the improved filter prototype. In addition, we also describe the results of verifying the performance requirements of the searchlight. As a result of the test and verification, the damage of the filter was improved and the improved filter was applied to the aircraft.