• Title/Summary/Keyword: 축류형

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Study on measuring the low torque on an air tool operating at 100,000 RPM class (100,000 RPM급으로 회전하는 에어공구에서의 저토오크 측정에 관한연구)

  • Kim, Eun-Jong;Cho, Soo-Yong
    • Proceedings of the KSME Conference
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    • 2003.04a
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    • pp.2018-2023
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    • 2003
  • An experiment is conducted for measuring the performance of an air tool, which is operated at 100,000 RPM at the unloaded state with the low torque. An experimental apparatus is developed as the power absorption type dynamometer. Inlet static pressure, flow rate, RPM and force are measured simultaneously. Torque, output power and specific output power are obtained. Those experimental results are compared with the experimental results obtained on a commercial dynamometer. However, no commercial dynamometers are available for measuring the torque above 30,000RPM. In order to use the commercial dynamometer, a reduction gear is applied to the shaft of dynamometer. Torque and power obtained on the commercial dynamometer show 50% lower than those obtained on a power absorption type dynamometer, because the inertia force is added to the air tool rotor for the braking system. Moreover, the starting RPM on the commercial dynamometer is less than 40,000RPM. From the compared results, they show that the power absorption type dynamometer should be applied for measuring the performance of an air tool operating at low torque and high RPM.

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Thermal Reliability Analysis of a Closed Type Motor in an Axial Fan for the Large Space Ventilation (대형공간환기용 축류팬에 사용되는 밀폐형 모터의 열신뢰성 분석)

  • Lee, Tae-Gu;Hur, Jin-Huek;Moon, Sun-Ae;Yoo, Ho-Seon;Moon, Seung-Jae;Lee, Jae-Heon
    • Proceedings of the SAREK Conference
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    • 2007.11a
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    • pp.494-499
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    • 2007
  • The thermal reliability of the closed-type BLDC motor for the high speed axial fans is analyzed by a numerical method in this dissertation. Since the module and the motor part are combined in a closed case, the heat generated from a rotor in the motor and the electronic components in the PCB module can not be effectively removed to the outside. Therefore the module will easily fail by high temperature. The accelerated-life testing was accomplished to formulate the life equation and numerical method is used to predict the inside temperature of the PCB module, which is one of the life equation parameter according to the environment. The experiment for measuring the surface heat flux of the electronic components is carried out to apply the boundary condition of numerical study. When the environment temperature of BLDC motor is 21, 35 and $50^{\circ}C$, the temperature in the PCB space is predicted as 73.4, 87.5 and $102.4^{\circ}C$. Then the life time with the temperature are calculated as 2,239, 863 and 328.

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A Study on Optimum Design of an Axial Cylcone structure using Response Surface Method (반응표면법을 활용한 축류형 사이클론 구조 최적화 설계에 관한 연구)

  • Cho, Jinill;Yun, Junho;Cho, Yeongkwang;Seok, Hyunho;Kim, Taesung
    • Particle and aerosol research
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    • v.17 no.3
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    • pp.71-79
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    • 2021
  • Ultrafine dust, which is emitted from industrial factories or all kinds of vehicles, threatens the human's respiratory system and our environment. In this regard, separating airborne particles is essential to mitigate the severe problem. In this work, an axial cyclone for the effective technology of eliminating harmful dust is investigated by numerical simulation using Ansys 2020, Fluent R2. In addition, the optimized structure of the cyclone is constructed by means of multi objective optimization based on the response surface method which is a representative method to analyze the effect of design parameter on response variables. Among several design parameters, the modified length of the vortex finder and dust collector is a main point in promoting the performance of the axial cyclone. As a result, the optimized cyclone exhibits remarkable performance when compared to the original model, resulting in pressure drop of 307 Pa and separator efficiency of 98.5%.

SMART 냉각재순환펌프 개념설계

  • Park, Jin-Seok;Heo, Hyeong;Kim, Jong-In;Kim, Ji-Ho;Koo, Dae-Hyun
    • Proceedings of the Korean Nuclear Society Conference
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    • 1998.05b
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    • pp.885-890
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    • 1998
  • SMART 냉각재순환펌프는 수직형 축류펌프로 분류되며 작동되는 환경의 특성상 캔드모터 펌프로 설계하였다. 냉각재순환점프의 전체 구조에 대한 개념설계를 수행하였으며 펌프의 주요부품인 회전측 집합체, 베어링 집합체, 전동기를 설계하였다. 베어링의 구조와 형상설계를 수행하였고 전동기는 농형유도 전동기로 설계하였으며 회전자의 슬롯에 대한 상세설계와 고정자의 슬롯에 대한 상세설계를 수행하였다. 앞으로 회전축의 동특성 해석, 임펠러의 캐비테이션 시험, 베어링의 내구성 시험, 펌프몸체의 응력해석을 수행할 예정이다.

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축류 압축기 기술 개발 동향

  • Song, Jae-Uk;Lee, Seong-Ryong;Lee, Sang-Eon
    • The KSFM Journal of Fluid Machinery
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    • v.12 no.5
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    • pp.61-65
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    • 2009
  • 현재 선진업체들은 성능과 구조적으로 경쟁력 있는 산업용 가스터빈 압축기를 설계하기 위하여 항공기용 압축기 설계기술을 전용하고 있다. 따라서 두산중공업은 DGT-5 압축기 익형설계를 위해 항공용 익형설계에 적용되는 S-Profile 설계기술을 활용하여 설계하였으며 현재 DGT-5 압축기에 대한 1차 성능시험이 완료되어 만족할 만한 결과를 얻었다. 그리고 DGT-5 압축기는 추후 두산중공업 파생형 가스터빈 압축기의 기본압축기로 활용할 계획이다.

Design of a Propeller Type Rim-Driven Axial-Flow Turbine for a Micro-Hydropower System (마이크로 수력 발전을 위한 프로펠러형 림구동 축류 터빈 설계)

  • Oh, Jin-An;Bang, Deok-Je;Jung, Rho-Taek;Lee, Su-Min;Lee, Jin-Tae
    • Journal of the Society of Naval Architects of Korea
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    • v.59 no.3
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    • pp.183-191
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    • 2022
  • A design method for a propeller type rim-driven axial-flow turbine for a micro-hydropower system is presented. The turbine consists of pre-stator, impeller and post-stator, where the pre-stator plays a role as a guide vane to provide circumferential velocity to the on-coming flow, and the impeller as a rotational power generator by absorbing angular momentum of the flow. BEM(Blade Element Method), which is based on the turbine Euler equation, is employed to design the pre-stator and impeller blades. NACA 66 thickness form and a=0.8 mean camber line, which is widely accepted as a marine propeller blade section, is used for the pre-stator and turbine blade section. A CFD method, derived from the discretization of the RANS equations, is applied for the analysis of the designed turbine system. The design conditions of the turbine is confirmed by the CFD calculation. Turbine characteristic curve is calculated by the CFD method, in order to provide the performance characteristics at off-design operation conditions. The proposed procedures for the design of a propeller type rim-driven axial-flow turbine are established and confirmed by the CFD analysis.

Optimization of flow performance by designing orifice shape of outdoor unit of air-conditioner (에어컨 실외기 냉각팬 시스템의 오리피스 형상 설계를 통한 유량 성능 최적화)

  • Ryu, Seo-Yoon;Kim, Sanghyeon;Cheong, Cheolung;Kim, Jong-Uk;Park, Byeong Il;Park, Se Min
    • The Journal of the Acoustical Society of Korea
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    • v.36 no.6
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    • pp.371-377
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    • 2017
  • The performance of an air conditioner is closely related to the cooling performance of a split-type outdoor unit so that, in most of the relevant preceding studies, the independent performance of an axial fan in an outdoor unit has been studied. However, there is a lack of research on the effects of other components in an outdoor units was rarely investigated. Therefore, in this paper, the effects of the fan orifice among other parts on the flow performance of the outdoor unit was numerically investigated. A virtual fan tester consisting of 18 million grids was developed for highly resolved flow simulation. The unsteady RANS (Reynolds-averaged Navier-Stokes) equations are numerically solved by using finite-volume CFD (Computational Fluid Dynamics) techniques. In order to verify the validity of the numerical methods, the predicted P-Q curve of the cooling fan in a full outdoor unit is compared with the measured one. Optimization of orifice shape was carried out for maximum flow performance of the outdoor unit using the validated numerical method.

Experimental Study on the Performance of Axial Flow Rotary Heat Exchanger with the Porous Polyurethane Foam Matrix (다공질 폴리우레탄 폼 매트릭스 축류 회전형 열교환기의 성능특성에 관한 실험적 연구)

  • Tae, C.S.;Park, S.D.;Cho, S.H.;Choi, Y.D.
    • Korean Journal of Air-Conditioning and Refrigeration Engineering
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    • v.5 no.1
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    • pp.44-54
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    • 1993
  • This is an experimental study to identify the performance of air-to-air rotary heat exchanger with polyurethane foam matrix. The experimental apparatus including heating AHU(Air Handling Unit), cooling AHU, sensor chamber, and heat exchanger testing unit was designed and manufactured in this study. The performance of heat exchanger with porous polyurethane foam matrix was tested with variations of the density and the thickness of matrix, regulating the wind velocity and the rotational speed of matrix. The actual heat recovery effectiveness, air leakage rate, and pressure drop of heat exchanger were measured and analyzed.

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Performance Design of Turbopump Type Liquid Rocket Engine System with Separate Flow Cycle (터보펌프 방식을 사용하는 개방형 가스발생기 사이클 로켓엔진의 성능설계)

  • Park Byunghoon;Yang Heesung;Kim Wonho;Ju Daesung;Yoon Woongsup
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • v.y2005m4
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    • pp.123-127
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    • 2005
  • LRE(liquid rocket engine) performance design code with several modules for each engine component has been developed for a preliminary design purpose. Thrust chamber, non-cryogenic centrifugal pump, single stage axial impulse turbine, gas generator and exhaust pipe for extra thrust have been considered. For simplicity, pump exit pressures are fixed, which eliminates pressure balancing problem between thrust chamber and turbopump unit. In this paper, calculated performance parameters with system flow charts and the design methodologies for each component are briefly presented and the results are compared with tile real engine specification.

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