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Design and Performance of a Catadioptric Omnidirectional Zoom Optical System Using a Hybrid Lens for Visible Light (가시광에서 하이브리드 렌즈를 사용한 반사굴절식 전방위 줌 광학계의 설계 및 성능평가)

  • Park, Hyun Sik;Jo, Jae Heung
    • Korean Journal of Optics and Photonics
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    • v.31 no.2
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    • pp.96-104
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    • 2020
  • A catadioptric omnidirectional zoom optical system using a hybrid lens (COZOSH) that performs simultaneously two functions of a lens and a mirror was designed at the visible wavelength range for daytime unmanned surveillance, and its performance was analyzed. The hybrid lens has lots of advantages in terms of fabrication and assembly of a COZOSH, because of the obviation of a lens boring process and reduction of the number of optical components. Additionally, we designed the COZOSH to expand the compressed inner-image region of a donut image at low spatial frequencies. As a result, the optimized design performance of the optical system that satisfies all initial design specifications was obtained from calculation of the modulation transfer function, spot diagram, and tolerance analysis. We confirmed that the COZOSH is a passively athermalized optical system under conditions of temperature variation from -30℃ to 50℃, by using athermalization analysis during zooming.

A Study on the Cause and Improvement of Crack in the Installing Structure of the Bulkhead of Aircraft (항공기 Bulkhead 체결구조의 균열 원인 및 개선에 관한 연구)

  • Choi, Hyoung Jun;Park, Sung Jae
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.21 no.6
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    • pp.448-454
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    • 2020
  • This study aims to determine the cause of structural defects occurring during aircraft operations and to verify the structural integrity of the improved features. The fracture plane was analyzed to verify the characteristics of the cracks and the fatigue failure leading to the final fracture was determined by the progress of the cracks by the repeated load. During aircraft operations, the comparative analysis of the load measurement data at the cracks with the aircraft design load determined that the measured load was not at the level of 30% of the design to be capable of being damaged. A gap analysis resulted in a significant stress of approximately 32 ksi at the crack site. Pre-Load testing also confirmed that the M.S. was reduced by more than 50% from +0.71 to +0.43, resulting in a sharp increase in aircraft load and the possibility of cracking when combined. Thus, structural reinforcement and the removal of the gap for aircraft cracking sites improved the defect. Based on the structural strength analysis of the improvement features, the bulkhead has a margin of about +0.88 and the fitting feature is about +0.48 versus allowable stress. In addition, the life analysis results revealed an improvement of approximately 84000 hours.