• Title/Summary/Keyword: 음향 불안정

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A study on combustion instability of solid rocket motor with cylinder-slot grain (실린더-슬롯형 그레인을 가진 고체로켓모터의 연소불안정 연구)

  • Lee, Dohyung;Kim, Hongjip
    • The Journal of the Acoustical Society of Korea
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    • v.39 no.4
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    • pp.371-377
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    • 2020
  • Combustion instability occurred in the combustion test of solid rocket motor with large aspect ration Length/Diameter (L/D) and cylinder-slot grain. As a result of spectral analysis of the pressure perturbation, it was confirmed that the central axis longitudinal frequency was dominant, so that the length of the cylinder part was increased to eliminate the coincidence with acoustic node. In addition, acoustic modal analysis and flow analysis were performed to analyze the cause of instability by unsteady flow structure in solid rocket motors. It was confirmed that the combustion instability is reduced by quantitative comparison of the amplitude and frequencies of the pressure inside the combustion chamber using the grain shape before and after the design change. Finally, a combustion test was performed to verify that the combustion instability was resolved as in the flow analysis.

A Numerical Study on Sensitivity of Acoustic Response to Pressure Oscillations in Liquid Rocket Engine (압력진동에 대한 액체 로켓엔진의 음향 응답의 민감도에 관한 수치적 연구)

  • Sohn, Chae-Hoon
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.30 no.5
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    • pp.79-87
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    • 2002
  • Acoustic responses to pressure oscillations in axisymmetric combustion chamber are numerically investigated to examine the qualitative trend of acoustic instability in liquid rocket engine. Chamber operating condition and excitation frequency of oscillating pressure are selected as exciting parameters of acoustic instability. Artificial perturbation is simulated by total-pressure oscillation with sine wave at chamber inlet. Many approximations and simplifications are introduced without losing the essence of acoustic pressure response. First, steady-state solution for each operating condition is obtained and next, transient analysis is conducted. Depending on operating condition and excitation frequency, the distinct response characteristics are brought. Weak-strength flames and high-frequency excitation tend to cause sensitive acoustic pressure response leading to unstable pressure field. These results are analyzed based on the correlation with acoustic pressure responses from the previous works adopting laminar flamelet model.

A Numerical Study on Acoustic Behavior in Combustion Chamber with Acoustic Cavity (음향공이 장착된 로켓엔진 연소실의 음향장 해석)

  • Sohn, Chae-Hoon;Kim, Young-Mog
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.30 no.4
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    • pp.28-37
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    • 2002
  • Acoustic behavior in combustion chamber with acoustoc cavity is numerically investigated by adopting linear acoustic analysis. Helmholtz-type resonator is employed as a cavity model to suppress acoustic instability passively. The tuning frequency of acoustic cavity is adjusted by varying the sound speed in acoustic cavity. Through harmonic analysis, acoustic pressure responses of chamber to acoustic oscillating excitation are shown and the resonant acoustic modes are identified. Acoustic damping effect of acoustic cavity is quantified by damping factor. As the tuning frequency approaches the target frequency of the resonant mode to be suppressed, mode split from the original resonant mode to lower and upper modes appears and thereby damping effect is degraded significantly. Considering mode split and damping effect as a function of tuning frequency, it is desirable to make acoustic cavity tuned to maximum frequency of those of the possible splitted upper modes.

An Experimental Study on Optimum Design of Half-Wave Resonators for Combustion Stabilization (연소 불안정 억제를 위한 반파장 공명기 최적 설계 조건에 대한 실험적 연구)

  • Park, Ju-Hyun;Sohn, Chae-Hoon
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.11a
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    • pp.11-14
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    • 2008
  • Acoustic design parameters of a half-wave resonator are studied experimentally for acoustic stability in a model acoustic tube. According to standard acoustic-test procedures, acoustic-pressure signals are measured. Quantitative acoustic properties of sound absorption coefficient are evaluated and thereby, the acoustic damping capacity of the resonator is characterized. The diameter and the number of a half-wave resonator and the diameter of the tube are selected as design parameters for optimal tuning of the resonator. Optimum acoustic damping capacity is observed at smaller open area ratio as the resonator diameter increases.

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The Nonlinear Combustion Instability Prediction of Solid Rocket Motors (고체로켓모터의 비선형 연소 불안정성 예측 기법)

  • Hong, Ji-Seok;Moon, Hee-Jang;Sung, Hong-Gye;Um, Won-Seok;Seo, Seonghyeon;Lee, Do-hyung
    • Journal of the Korean Society of Propulsion Engineers
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    • v.20 no.1
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    • pp.20-27
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    • 2016
  • The prediction of combustion instability is important to avoid an obvious threat to the structural safety and the motor performance because it affects the apparent response function of the propellant, the burning rate, and a mean flow Mach number at the local surface. The combustion instability occurs in case acoustic waves were coupled with the combustion/flow dynamic frequency. In this paper, an acoustic instability model is derived from the nonlinear wave equation for analysing acoustic dynamics in solid rocket motors. The chamber pressure and burning rate effects on combustion instability have been investigated.

Development of Helmholtz Solver for Thermo-Acoustic Instability within Combustion Devices (연소시스템의 열음향 불안정 예측을 위한 Helmholtz Solver 개발)

  • Kim, Seong-Ku;Choi, Hwan-Seok;Cha, Dong-Jin
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.38 no.5
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    • pp.445-455
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    • 2010
  • In order to effectively predict thermo-acoustic instability within real combustors of rocket engines and gas turbines, in the present study, the Helmholtz equation in conjunction with the time lag hypothesis is discretized by the finite element method on three-dimensional hybrid unstructured mesh. Numerical nonlinearity caused by the combustion response term is linearized by an iterative method, and the large-scale eigenvalue problem is solved by the Arnoldi method available in the ARPACK. As a consequence, the final solution of complex valued eigenfrequency and acoustic pressure field can be interpreted as resonant frequency, growth rate, and modal shape for acoustic modes of interest. The predictive capabilities of the present method have been validated against two academic problems with complex impedance boundary and premixed flame, as well as an ambient acoustic test for liquid rocket combustion chamber with/without baffle.

Damping Characteristic of Helmholtz Resonator according to Its Geometry and Sound Pressure Level (헬름홀쯔 공명기의 기하학적 형상과 가진 음압에 따른 감쇠 특성)

  • Song, Jae-Kang;Kim, Ki-Woo;Chae, Byoung-Chan;Ko, Young-Sung;Kim, Sun-Jin
    • Journal of the Korean Society for Aeronautical & Space Sciences
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    • v.38 no.10
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    • pp.966-972
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    • 2010
  • Damping characteristics of a Helmholtz resonator to passively control the combustion instability were investigated by linear acoustic analysis and atmospheric acoustic tests. Its orifice length and diameter were selected as the design parameters and supplied SPL(sound pressure level) effect on damping characteristics were investigated. Damping capacity is improved by decreasing the orifice length as well as by increasing the orifice diameter. Also, the results showed that the damping capacity of the resonator decreased nonlinearly about above 110 dB and instabilities in the nonlinear region were more effectively suppressed by increasing the orifice diameter.

Damping Characteristics of a Helmholtz Resonator Under the Flow Area (튜브(모사 챔버)내의 유동특성이 음향공 감쇠 능력에 미치는 영향)

  • Song, Jae-Gang;Kim, Young-Mun;Ko, Young-Sung;Kim, Sun-Jin
    • Proceedings of the Korean Society of Propulsion Engineers Conference
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    • 2008.11a
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    • pp.82-85
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    • 2008
  • A Helmholtz resonator is applied to control high frequency combustion instability in liquid rocket engine. Damping characteristics of the Helmholtz resonator are investigated by the flow characteristic and its design. To simulate combustion instability, resonance in a test section(with fixed volume) is made by a pressure pulsator, and then damping characteristics are investigated. Its orifice length and diameter are selected as the design parameters and flow rates are varied to reveal the effect on damping characteristics. The experimental results show that a Helmholtz resonator is also working with flows. When length and diameter of an orifice are small, the tuning frequency increases as the flow velocity increases.

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Open-Loop Control of Combustion Instability in Hot-Firing Test Using Gaseous Hydrocarbon Fuel (기체 탄화수소 연료 연소시험에서 연소불안정의 개루프 제어)

  • Hwang, Donghyun;Ahn, Kyubok
    • Journal of the Korean Society of Propulsion Engineers
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    • v.22 no.6
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    • pp.28-36
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    • 2018
  • A study was conducted to apply open-loop control to the combustion instability in a dump combustor using gaseous hydrocarbon fuels. Control power and frequency were varied by employing a loudspeaker under combustion conditions with similar characteristic chemistry times of the fuels. In the case of open-loop control where the frequency was identical to the combustion instability frequency, the open-loop control power affected the control performance. Results obtained from conducted open-loop control tests, where the frequency was different from the combustion instability frequency, show that setting the open-loop control frequency similar to the combustion instability frequency is effective.

2-Parameter High Frequency Combustion Instability Model (2-파라메타 모델에 의한 고주파 연소불안정 해석)

  • 조용호;윤웅섭
    • Journal of the Korean Society of Propulsion Engineers
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    • v.1 no.2
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    • pp.74-83
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    • 1997
  • The definition of burning admittance and conventional n-$\tau$ stability rating technique are combined to investigate the high frequency combustion instabilities inside the cylindrical combustion chamber. Perturbed flow variables are written as the sum of fluctuating and time-averaged mean quantities on the assumption that the terms of the order higher than unity are sufficiently small, hence linearized governing equations could be formulated. Chamber admittances up and downstream of the flame front calculated with appropriate boundary conditions result in the burning admittance and corresponding n-$\tau$ neutral stability curve. Configurational and operational design factors are tested to detect the unstable wave-induced LOX-RP1 combustion instabilities. Operational design factors, e.g. pressure or O/F ratio, appear less influential to drive high frequency instability while the location of the flame front and configurational factors enhance or deteriorate the stabilities strongly. Conclusively, LOX-RP1 combustion inside the cylindrical combustion chamber is apt to be unstable against long residence time and shortened chamber length.

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