• Title/Summary/Keyword: 석탄 전환율

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The operation Characteristic of Pilot-scale 2-Stage Coal gasifier (Pilot 규모 2단 형상 가스화기 운전특성 실험)

  • Hong, Jin-Pyo;Chung, Jae-Hwa;Seo, Seok-Bin;Chi, Jun-Hwa;Lee, Seung-Jun;Chung, Suk-Woo
    • 한국신재생에너지학회:학술대회논문집
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    • 2009.11a
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    • pp.528-532
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    • 2009
  • Integrated Gasification Combined Cycle (IGCC) power plant converts coal to syngas, which is mainly composed with hydrogen and carbon monoxide, by the gasification process and produces electric power by the gas and steam turbine combined cycle power plant. The purpose of this study is to investigate the influence of gasification process to type and structure of gasifier. For this purpose, the performance characteristics of gasification reaction are analyzed with the operation characteristic of pilot-scale 2-stage coal gasifier. It is found that gasification reaction, floating characteristic of melted slag, particle stick of inside of the gasifier, particle stick and deposit of Syngas cooler are the causes in the different performance characteristics.

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Combustion Characteristics of Imported Bituminous & Subbituminous Coal in a Pilot Scale Test Facility (발전용 역청탄 및 아역청탄의 파일롯 연소특성 평가)

  • Kim, Hyunhee;Park, Hoyoung;Lim, Hyunsoo;Baek, Sehyun;Kim, Taehyung;Kim, Youngju;Gong, Jiseon;Lee, Jeongeun
    • Journal of Energy Engineering
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    • v.23 no.4
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    • pp.207-214
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    • 2014
  • With the depletion of high grade coal, it is indispensable to be used co-combustion of low rank coal with bituminous coal in pulverized coal-fired power plants. This study describes the detailed measurements of combustion characteristics of bituminous and subbituminous coal in a 0.7MWth pilot-scale test facility. This experimental works include the measurement of gas temperature, gas concentrations along with the reactor axial and radial distance at the condition of excess air ratio of 1.2. The solid sampling was carried out and analyzed with the combustion of bituminous coal. The main reaction zone of coal flame in a reactor was formed about 1 m from the swirl burner, and at downstream, the fully developed temperature and species distribution was observed. The sampled particles of bituminous coal in a reactor revealed the complete carbon burn-out was achieved just after an main combustion zone.

전기연구소설립을 촉구함

  • 양재권
    • 전기의세계
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    • v.24 no.4
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    • pp.3-5
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    • 1975
  • 우리 인간은 그들이 개발한 과학과 기술에 의하여 자연 중에 존재하는 많은 자원을 그들의 생활에 도움이 되는 물체로 바꾸어 왔고 각종 에너지를 그들이 필요로 하는 형태로 바꾸었으며 또 그들이 사는 환경을 더욱 안락하도록 개조하여 왔다. 인간에 계속해서 현재와 같이 생활상태를 향상시키며 번영을 시도한다면 과학기술개발은 영원히 계속될 것이다. 이 과학기술개발에 관한 노력은 과거에는 가치관의 차이로 국가간의 노력의 차이가 있었으나 현재는 선후진국을 막론하고 과학기술에 의한 공업진흥이 국가사회의 경제개발의 원동력이며 그 생활향상의 열쇠가 된다는 것을 다 깨닫고 있다. 이와 같은 과학기술과 인간생활과의 숙명적인 관계중에서도 전기학술과 인간관계는 타과학과의 관계보다 훨씬 깊은 바가 있다. 우리는 호수에 물의 위치 에너지, 석탄이 가지고 있는 열에너지, 바람이 가지고 있는 운동에너지 등을 비롯하여 최근에 발견된 원자에너지까지도 이를 전기에너지로 변환시켜서 이용하고 있다. 장래 어떠한 에너지가 새로 개발되더라도 전기에너지로 변환되어 현재와 같이 우리 생활에 기여할 것은 틀림없다. 이는 전기에너지의 사용편리성으로 볼 때 이의를 제기할 사람은 없을 것이다. 따라서 각종에너지를 전기에너지로 바꾸는 발전기술과 이 장치의 제조공업, 이를 수요지까지 수송하는 송변전기술과 이 장치의 제조공업, 공장에서 사용되는 전기기기들의 운전사용기술과 가정에서 소요되는 전기기기의 제조공업 이상 전기공업의 여러 방치에 소요되는 원자재의 제조공업 등 소위 전기기술은 인간생활과 절대 불가분의 기술이며 앞으로도 인류의 존재와 더불어 영원한 발전을 계속할 것이다. 전기기술발전없이 인간사회와 국가의 산업발전을 기대한다는 것은 어리석은 일이라 아니할 수 없다. 가까운 장래 우리나라 계통이 당면하여야 할 계통제어에 관한 몇가지 문제를 고찰하고저 한다. 단 개개의 문제에 관한 구체적인 해석 또는 검토에 관하여는 다음 기회에 미루기로하고, 우선 여기서는 당면문제로서 대처하지 않으면 안될 자동주파수제어문제및 계통의 경제운용문제만에 한정하여, 이것을 우리나라의 현상과 관련시켜 개설하고, 이들의 자동화에 관한 기본적인 문제를 간단히 적어 보겠다. 가능하다. 제작완료된 ASIC은 기능시험을 완료했으며 실제 line-of-sight(LOS) 시스템 구현에 적용중이다. 시대를 살아 갈 회원들이다. '컨텐츠의 시대'가 개막되는 것이며, 신세기통신과 SK텔레콤은 선의의 경쟁 과 협력을 통해 이동인터넷 서비스의 컨텐츠를 개발해 나가게 될 것이다. 3배가 높았다. 효소 활성에 필수적인 물의 양에 따른 DIAION WA30의 라세미화 효율에 관하여 실험한 결과, 물의 양이 증가할수록 그 효율은 감소하였다. DIAION WA30을 라세미화 촉매로 사용하여 아이소옥탄 내에서 라세믹 나프록센 2,2,2-트리플로로에틸 씨오에스터의 효소적 DKR 반응을 수행해 보았다. 그 결과 DIAION WA30을 사용하지 않은 경우에 비해 반응 전환율과 생성물의 광학 순도는 급격히 향상되었다. 전통적 광학분할 반응의 최대 50%라는 전환율의 제한이 본 연구에서 찾은 DIAION WA30을 첨가함으로써 성공적으로 극복되었다. 또한 고체 염기촉매인 DIAION WA30의 사용은 라세미화 촉매의 회수 및 재사용이 가능하게 해준다.해준다.다. TN5 세포주를 0.2 L 규모 (1 L spinner flask)oJl에서 세포간의 응집현상 없이 부유배양에 적응,배양시킨 후 세포성장 시기에 따른 발현을 조사한 결과 1 MOI의

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Kinetic study on Low-rank Coal Including K2CO3, Na2CO3, CaCO3 and Dolomite Gasification under CO2 Atmosphere (이산화탄소 분위기에서 K2CO3, Na2CO3, CaCO3 및 Dolomite가 첨가된 저급탄의 가스화에 대한 반응특성연구)

  • Hwang, Soon Choel;Kim, Sang Kyum;Park, Ji Yun;Lee, Do Kyun;Lee, Si Hyun;Rhee, Young Woo
    • Clean Technology
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    • v.20 no.1
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    • pp.64-71
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    • 2014
  • We have investigated the effects of various additives on Eco coal gasification under $CO_2$ atmosphere. The temperature ranges from $750{\sim}900^{\circ}C$ and the gasification experimental was carried out with Eco coal adding 7 wt% $K_2CO_3$, $Na_2CO_3$, $CaCO_3$, Dolomite, and non-additive under $N_2$ and $CO_2$ gas mixture. At $850^{\circ}C$, we observed that the reaction rate increased when the concentration of $CO_2$ increased. However, we also observed that the increment of reaction rate was small at more than 70% of the concentration of $CO_2$. The additives activity was ranked as 7 wt% $Na_2CO_3$ > 7 wt% $K_2CO_3$ > non-additive > 7 wt% Dolomite > 7 wt% $CaCO_3$ at $850^{\circ}C$. At the temperatures of $750^{\circ}C$, $800^{\circ}C$, $850^{\circ}C$, and $900^{\circ}C$, when the temperature increased, the gasification rate increased. The gasification was suitably described by the volumetric reaction model. Using volumetric reaction model, the activation energy of Eco coal including 7 wt% $Na_2CO_3$ gasification was 83 kJ/mol, which was the lowest value among all the alkaline additives.

SO2 Reduction with CO over SnO2-ZrO2(Sn/Zr=2/1) Catalyst for Direct Sulfur Recovery Process with Coal Gas: Optimization of the Reaction Conditions and Effect of H2O Content (석탄가스를 이용한 직접 황 회수공정을 위한 SnO2-ZrO2(Sn/Zr=2/1) 촉매 상에서의 CO에 의한 SO2 환원 반응: 반응조건 최적화 및 수분의 영향)

  • Han, Gi Bo;Shin, Boo-Young;Lee, Tae Jin
    • Applied Chemistry for Engineering
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    • v.18 no.2
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    • pp.155-161
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    • 2007
  • In this study, the reactivity of a $SnO_2-ZrO_2$(Sn/Zr = 2/1) catalyst for $SO_2$ reduction by CO was investigated in order to optimize the various reaction conditions such as temperature, gas hourly space velocity (GHSV), and [CO]/[$SO_2$] molar ratio. The reaction temperature in the range of $300{\sim}550^{\circ}C$, space velocity in the range of $5000{\sim}30000cm^3/[g_{-cat}{\cdot}h]$ and [CO]/[$SO_2$] molar ratio in the range of 1.0~4.0 were employed. The optimum temperature, GHSV, and [CO]/[$SO_2$] molar ratio were determined to be $325^{\circ}C$, $10000cm^3/[g_{-cat}{\cdot}h]$, and 2.0, respectively; under these conditions, $SO_2$ conversion was over 99% and sulfur selectivity was over 95%. In addition, the effect of $H_2O$ content on the $SO_2$ reduction by CO was also investigated. As the $H_2O$ content increased from 2 vol% up to 6 vol%, the reactivity and sulfur selectivity decreased. In case of 2 vol% $H_2O$ content, the reaction temperature and [CO]/[$SO_2$] molar ratio were varied in the range of $300{\sim}400^{\circ}C$ and 1.0~3.0. The optimum temperature and [CO]/[$SO_2$] molar ratio were $340^{\circ}C$ and 2.0, respectively under which $SO_2$ conversion and sulfur selectivity were about 90% and 87%, respectively.

Study on the Co-firing of Sewage Sludge to a 80 kWth-scale Pulverized Coal Combustion System (80 kWth급 미분탄 연소 시스템에서 하수슬러지 혼소시 연소 특성 연구)

  • Chae, Taeyoung;Lee, Jaewook;Lee, Youngjae;Yang, Won
    • Clean Technology
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    • v.25 no.1
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    • pp.74-80
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    • 2019
  • Thermochemical treatment of sewage sludge is an energy-intensive process due to its high moisture content. To save the energy consumed during the process, the hydrothermal carbonization process for sewage sludge can be used to convert sewage sludge into clean solid fuel without pre-drying. This study is aimed to investigate co-firing characteristics of the hydrothermally carbonated sewage sludge (HCS) to a pulverized coal combustion system. The purpose of the measurement is to measure the pollutants produced during co-firing and combustion efficiency. The combustion system used in this study is a furnace with a down-firing swirl burner of a $80kW_{th}$ thermal input. Two sub-bituminous coals were used as a main fuel, and co-firing ratio of the sewage sludge was varied from 0% to 10% in a thermal basis. Experimental results show that $NO_x$ is 400 ~ 600 ppm, $SO_x$ is 600 ~ 700 ppm, and CO is less than 100 ppm. Experimental results show that stable combustion was achieved for high co-firing ratio of the HCS. Emission of $NO_x$ and $SO_x$ was decreased for higher co-firing ratio in spite of the higher nitrogen contents in the HCS. In addition, it was found that the pollutant emission is affected significantly by composition of the main fuel, regardless of the co-firing ratios.

Kinetic of Catalytic CO2 Gasification for Cyprus Coal by Gas-Solid Reaction Model (기-고체 반응모델을 이용한 Cyprus탄의 CO2 저온촉매가스화 반응거동)

  • Hwang, Soon Choel;Lee, Do Kyun;Kim, Sang Kyum;Lee, Si Hyun;Rhee, Young Woo
    • Korean Chemical Engineering Research
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    • v.53 no.5
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    • pp.653-662
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    • 2015
  • In general, the coal gasification has to be operated under high temperature ($1300{\sim}1400^{\circ}C$) and pressure (30~40 bar). However, to keep this conditions, it needs unnecessary and excessive energy. In this work, to reduce the temperature of process, alkali catalysts such as $K_2CO_3$ and $Na_2CO_3$ were added into Cyprus coal. We investigated the kinetic of Cyprus char-$CO_2$ gasification. To determine the gasification conditions, the coal (with and without catalysts) gasified with fixed variables (catalyst loading, catalytic effects of $Na_2CO_3$ and $K_2CO_3$, temperatures) by using TGA. When catalysts are added by physical mixing method into Cyprus coal the reaction rate of coal added 7 wt% $Na_2CO_3$ is faster than raw coal for Cyprus char-$CO_2$ gasification. The activation energy of coal added 7 wt% $Na_2CO_3$ was calculated as 63 kJ/mol which was lower than raw char. It indicates that $Na_2CO_3$ can improve the reactivity of char-$CO_2$ gasification.

Kinetic Study on Char-CO2 Catalytic Gasification of an Indonesian lignite (인도네시아 갈탄의 촤-CO2 촉매가스화 반응특성연구)

  • Lee, Do Kyun;Kim, Sang Kyum;Hwang, Soon Choel;Lee, Si Hoon;Rhee, Young Woo
    • Korean Chemical Engineering Research
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    • v.52 no.4
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    • pp.544-552
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    • 2014
  • In this study, We have investigated the kinetics on the char-$CO_2$ gasification reaction. Thermogravimetric analysis (TGA) experiments were carried out for char-$CO_2$ catalytic gasification of an Indonesian Roto lignite. $Na_2CO_3$, $K_2CO_3$, $CaCO_3$ and dolomite were selected as catalyst which was physical mixed with coal. The char-$CO_2$ gasification reaction showed rapid an increase of carbon conversion rate at 60 vol% $CO_2$ and 7 wt% $Na_2CO_3$ mixed with coal. At the isothermal conditions range from $750^{\circ}C$ to $900^{\circ}C$, the carbon conversion rates increased as the temperature increased. Three kinetic models for gas-solid reaction including the shrinking core model (SCM), volumetric reaction model (VRM) and modified volumetric reaction model (MVRM) were applied to the experimental data against the measured kinetic data. The gasification kinetics were suitably described by the MVRM model for the Roto lignite. The activation energies for each char mixed with $Na_2CO_3$ and $K_2CO_3$ were found a 67.03~77.09 kJ/mol and 53.14~67.99 kJ/mol.

The Study on the Catalytic Performance and Characterization of La0.9Sr0.1Cr0.7B0.3O3±δ (B=Mn, Ni, Fe, Ru) for High Temperature Water-gas Shift Reaction with Simuated Coal-derived Syngas (모사된 석탄가스화 합성가스를 이용한 La0.9Sr0.1Cr0.7B0.3O3±δ (B=Mn, Ni, Fe, Ru)의 수성가스전이반응 활성 및 특성에 관한 연구)

  • Lee, Seul-Gi;Kwak, Jaehoom;Sohn, Jung Min
    • Transactions of the Korean hydrogen and new energy society
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    • v.24 no.6
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    • pp.543-549
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    • 2013
  • In this study, $La_{0.9}Sr_{0.1}Cr_{0.7}M_{0.3}O_{3{\pm}{\delta}}$ (M=Mn, Ru, Fe, Ni) were prepared by sol-gel method and water gas shift reaction with simulated coal-derived syngas between $400{\sim}650^{\circ}C$ was conducted to evaluate the catalytic activity of prepared catalysts. Physico-chemical properties were characterized by XRD, BET, SEM-EDS and TPR. The formation of perovskite crystallite, $LaCrO_3$ was confirmed and the highest surface area was measured with $La_{0.9}Sr_{0.1}Cr_{0.7}Mn_{0.3}O_{3{\pm}{\delta}}$. Equilibrium conversion of CO above $550^{\circ}C$ was achieved except $La_{0.9}Sr_{0.1}Cr_{0.7}Fe_{0.3}O_{3{\pm}{\delta}}$. and methanation reaction was carried out as side reaction of water gas shift reaction with $La_{0.9}Sr_{0.1}Cr_{0.7}Ni_{0.3}O_{3{\pm}{\delta}}$ and $La_{0.9}Sr_{0.1}Cr_{0.7}Ru_{0.3}O_{3{\pm}{\delta}}$. Conclusively, $La_{0.9}Sr_{0.1}Cr_{0.7}M_n{0.3}O_{3{\pm}{\delta}}$ was the most suitable catalyst of water gas shift reaction above $500^{\circ}C$ for CO conversion and hydrogen production.

The Characteristics of Microbial Community for Biological Activated Carbon in Water Treatment Plant (생물활성탄 공정에서 활성탄 재질에 따른 부착미생물 군집특성)

  • Son, Hee-Jong;Park, Hong-Ki;Lee, Soo-Ae;Jung, Eun-Young;Jung, Chul-Woo
    • Journal of Korean Society of Environmental Engineers
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    • v.27 no.12
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    • pp.1311-1320
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    • 2005
  • The purpose of this research is to survey characteristics of microbial community and the removal efficiency of organic materials for biological activated carbon in water treatment plant. Coal based activated carbon retained more attached bacterial biomass on the surface of the activated carbon than the other activated carbon with operating time and materials. The heterotrophic plate count(HPC), eubacteria(EUB) and 4,6-diamidino-2-phenylindole(DAPI) counts were ranged from $0.95{\times}10^7$ to $52.4{\times}10^7$ CFU/g, from $3.8{\times}10^8$ to $134.2{\times}10^8$ cells/g and from $7.0{\times}10^8$ to $250.2{\times}10^8$ cells/g, respectively. The biomass of EUB and DAPI appeared to be much more $10^2$ than HPC, which were increasing in bed volume of 20,000 at the stage of steady-state. The change of microbial community by analyzing fluorescent in situ hybridization(FISH) method with rRNA-targeted oligonucleotide probes, the dominant group was $\alpha$-proteobacteria($\alpha$ group) and high G+C content bacteria(HGC) the lowest distributing rate before reaching the bed volume of 20,000. After reaching the bed volume of 20,000, $\alpha$ group and other groups of bacteria became decreased, on the other hand, the proportion of both $\beta$-proteobacteria($\beta$ group) and $\gamma$-proteobacteri($\gamma$ group) were increasing. Coconut and wood based activated carbons had similar trend with coal based activated carbon, but the rate of $\alpha$ group on coal based activated carbon had gradually increased. Bacterial production with the operating period appeared highest in coal based activated carbon at the range of $1.2{\sim}3.4\;mg-C/m^3{\cdot}h$ while the coconut and wood based activated carbon were ranged from 1.1 to 2.6 $mg-C/m^3{\cdot}h$ and from 0.7 to 3.5 $mg-C/m^3{\cdot}h$ respectively. The removal efficiency of assimilable organic carbon(AOC) showed to be highly correlated with bacterial production. The correlation coefficient between removal efficiency of AOC and bacterial production were 0.679 at wood based activated carbon, 0.291 at coconut based activated carbon and 0.762 at coal based activated carbon, respectively.