• Title/Summary/Keyword: 비연료소모율

Search Result 30, Processing Time 0.029 seconds

EASY5$^{\circledR}$ Modeling of Turboprop Engine for the Performance Analysis (성능해석을 위한 터보프롭엔진의 EASY5$^{\circledR}$ 모델링)

  • 최인수;기자영;공창덕
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2001.04a
    • /
    • pp.69-72
    • /
    • 2001
  • 본 연구에서는 터보프롭엔진의 성능해석 프로그램을 EASY5를 이용하여 최초로 시행하였다. 개발된 프로그램을 입증하기 위해 고도와 마하수를 고정한 상태에서 공기유량과 보기류 구동을 위한 출력손실의 변화에 따른 성능을 분석하였다. 해석 결과, Bleed 공기유량 손실과 보기류 구동을 위한 출력 손실에 의해 가용출력은 최대 6%의 손실을 보이나 비연료 소모율은 거의 영향을 미치지 않음을 알 수 있었다. 또한 EASY5 프로그램과 GASTURB 프로그램의 결과 비교에서도 최대 오차율 1.37% 이내에서 일치함을 확인할 수 있었다.

  • PDF

A Study on Steady-state and Transient Performance Simulation of Turboprop Engine(PT6A-62) (터보프롭엔진(PT6A-62)의 정.동적 성능모사에 관한 연구)

  • 공창덕;기자영;신현기
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.4 no.2
    • /
    • pp.61-70
    • /
    • 2000
  • The performance simulation program on the turboprop engine(PT6A-62), which is a main engine of the first trainer KT-1 in republic of Korea, was developed. Characteristics of engine components were required for the steady-state performance analysis including on and off design point analysis. In most cases, these were substituted for what scaled from well known engine components characteristics with the scaling law. The developed program was compared with CASTURB program which is well known for the simulation performance analysis, such as analysis results of mass flow rate, compressor pressure ratio, fuel flow rate, power, specific fuel consumption ratio and turbine inlet temperature in the following four cases, to evaluate whether the developed program is acceptable or not. The first case was the sea level static standard condition and other cases were considered with various flight Mach numbers, altitudes. After verifying the developed program, the partload performance analysis was carried out. Transient performance analysis for various fuel schedules were performed. When the fuel step increase of 0.1sec was performed, the overshoot of the compressor turbine inlet temperature occurred. However, the fuel ramp increase for longer than 0.1sec time was performed, the overshoot could be eliminated.

  • PDF

Detection Method of Vehicle Fuel-cut Driving with Deep-learning Technique (딥러닝 기법을 이용한 차량 연료차단 주행의 감지법)

  • Ko, Kwang-Ho
    • Journal of the Korea Convergence Society
    • /
    • v.10 no.11
    • /
    • pp.327-333
    • /
    • 2019
  • The Fuel-cut driving is started when the acceleration pedal released with transmission gear engaged. Fuel economy of the vehicle improves by active fuel-cut driving. A deep-learning technique is proposed to predict fuel-cut driving with vehicle speed, acceleration and road gradient data in the study. It's 3~10 of hidden layers and 10~20 of variables and is applied to the 9600 data obtained in the test driving of a vehicle in the road of 12km. Its accuracy is about 84.5% with 10 variables, 7 hidden layers and Relu as activation function. Its error is regarded from the fact that the change rate of input data is higher than the rate of fuel consumption data. Therefore the accuracy can be better by the normalizing process of input data. It's unnecessary to get the signal of vehicle injector or OBD, and a deep-learning technique applied to the data to be got easily, like GPS. It can contribute to eco-drive for the computing time small.

The Characteristics and Prospects of Hybrid Propulsion Systems for Unmanned Aerial Vehicle (무인기용 하이브리드 추진시스템의 특성 및 발전전망)

  • Park, Tosoon;Song, Jaeho;Kwon, Sejin
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2017.05a
    • /
    • pp.554-559
    • /
    • 2017
  • Recently, the global attention is focused on the development of the renewal aero-propulsion systems proved in the air pollution, the noise, the great operational cost, safety and risks. Especially, various study are conducting for the development of the advanced high power to weight ratio aircraft through the significant reduction of fuel consumption and upgrade of the propulsion efficiency, using the alternative propulsion system developments such as hydrogen and solar power system. The hybrid propulsion system can be the representative propulsion system which get the power sources by combining the merits of two or more power sources. In this study, the advancement trends, characteristics, design method which can be applied to the renewal future UAV development.

  • PDF

Measurement Uncertainty Assessment of Altitude Performance Test for a Turboshaft Engine (터보샤프트 엔진 고공성능시험의 측정 불확도 평가)

  • Yang, In-Young;Lee, Bo-Hwa
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.14 no.4
    • /
    • pp.59-64
    • /
    • 2010
  • Measurement uncertainty assessment was performed for altitude performance test for a turboshaft engine. Mathematical models of measurement were suggested for major performance parameters such as shaft horse power, fuel flow, specific fuel consumption, and airflow. The procedure was compared with the test of turbojet or turbofan engines. Uncertainty involved with the test condition measurement was assessed. Influence of the test condition measurement uncertainty on the corrected performance data was discussed. Uncertainty assessment result was provided for a example test case using a real altitude test facility. For major performance parameters, measurement uncertainties were assessed as 0.65~1.09% including the test condition measurement uncertainty, 0.36~0.94% not including it.

Study on the Humidity Effect on Gas turbine Engine Performances (습도가 엔진성능에 미치는 영향에 대한 실험적 고찰)

  • Lee, Bo-Hwa;Lee, Kyung-Jae;Yang, Soo-Seok;Kim, Chun-Taek
    • Aerospace Engineering and Technology
    • /
    • v.9 no.2
    • /
    • pp.98-104
    • /
    • 2010
  • The moisture in the atmosphere exerts a lot of influence upon Gas turbine engine performances. There is a noticeable influence of wet air at the summer sea level, high flight mach number and low engine rpm increasingly. An altitude Engine Test Facility is used to accomplish the engine performance tests at dry air condition and wet air condition, through which engine performance results is revealed. Also, Gas turbine Simulation Program is used to predict the variation of engine performance due to inlet humidity. In the result, net thrust and specific fuel consumption measured -2.826% and 1.325%, respectively at wet air condition compared to dry air condition.

Study on Performance and Optimal Operating Conditions of Regenerative Steam-Injection Gas Turbine Systems (증기분사 재생 가스터빈 시스템의 성능 및 최적 운전조건에 관한 연구)

  • Kim, Kyoung-Hoon;Kim, Dong-Joo;Park, Sang-Hee;Oh, Man-Soo;Kim, Dong-Myoung
    • Journal of the Korean Society of Propulsion Engineers
    • /
    • v.14 no.1
    • /
    • pp.29-39
    • /
    • 2010
  • The system performance of the regenerative gas-turbine cycle with the steam injection into the combustor has been studied through the thermodynamic cyclic analysis. The effects of the pressure ratio, the steam injection ratio, the ambient temperature, and the turbine inlet temperature are investigated on the thermal efficiency, the fuel consumption, and the specific power as well as the operating conditions for the maximum thermal efficiency of the system. The results of the present analysis find that the use of steam injection in the regenerative gas-turbine system can greatly enhance the thermal efficiency and the specific power of the system.

The introduction of Engine Performance Test for Miniature Turbojet Engine considering humidity effects (습도 영향을 고려한 초소형 터보제트 엔진 성능시험 소개)

  • Lee, Bo-Hwa;Lee, Kyung-Jae;Yang, Soo-Seok;Kim, Yu-Il
    • Proceedings of the Korean Society of Propulsion Engineers Conference
    • /
    • 2010.11a
    • /
    • pp.335-338
    • /
    • 2010
  • The moisture in the atmosphere exerts a lot of influence upon Gas turbine engine performances. There is a noticeable influence of wet air at the summer sea level, high flight mach number and low engine rpm increasingly. An altitude Engine Test Facility is used to accomplish the engine performance tests at dry air condition and wet air condition, through which engine performance results is revealed. In the result, net thrust and specific fuel consumption measured -2.826% and 1.325%, respectively at wet air condition compared to dry air condition.

  • PDF

A Study on the Characteristics of FDS Heat Release Rate Predictions for Fire involving Solid Combustible Materials in a Closed Compartment (밀폐된 구획 내 복합소재 고체 가연물의 연소시 열방출률의 FDS 예측 특성)

  • Hong, Ter-Ki;Roh, Beom-Seok;Park, Seul-Hyun
    • Journal of the Korea Academia-Industrial cooperation Society
    • /
    • v.21 no.11
    • /
    • pp.349-356
    • /
    • 2020
  • The heat release rate (HRR) and fire growth rate of fire for the solid combustibles consisting of multi-materials was measured through the ISO 9705 room corner test, and the computational analysis in a closed compartment was performed to simulate a fire using the heat release rate prediction model provided by a Fire Dynamics Simulator (FDS). The method of predicting the heat release rate provided by the FDS was divided into a simple model and a pyrolysis model. Each model was applied and computational analysis was performed under the same conditions. As the solid combustible consisting of multi-materials, a cinema chair composed mostly of PU foam, PP, and steel was selected. The simple model was over-predicted compared to the predicted heat release rate and fire growth rate using the pyrolysis model in a closed compartment.

A Study on the Emission and Particulate Matter of a Heavy Duty Natural Gas Engine According to Gas Composition under certification tests (인증시험 조건에서 가스조성 변화에 따른 대형 천연가스 엔진 배기가스 및 입자상 물질 배출 특성에 관한 연구)

  • Choi, Ji-Seon;Park, Cheol-Woong;Jang, Hyoung-Jun;Kim, Chang-Gi
    • Journal of the Korean Institute of Gas
    • /
    • v.25 no.6
    • /
    • pp.66-73
    • /
    • 2021
  • In this study, The full load test and WHTC mode test were performed to examine the effect on a heavy duty natural gas engine according to the type of standard gas for certification to check engine performance and exhaust characteristics. Two types of standard gas (Gr, G23) and commercially available natural gas were applied as the fuel used. As a result of the test results of three natural gases with different fuel compositions, G23 with a high nitrogen content was inferior in torque, fuel consumption, and thermal efficiency conditions. In addition, when evaluated in the WHTC mode it was possible to obtain a result that satisfies the EURO VI regulation. However, compared to the other two fuels, the emission characteristics of G23 decreased CO2 and CO, but increased CH4, NOx and PN emissions.