• Title/Summary/Keyword: 버핑

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Development of 5-Axis Microscribe System for Off-Line Buffing Robot Path Programming and Its Application (버핑 로봇의 오프라인 경로 프로그래밍용 5축 마이크로스크라이브 개발 및 응용)

  • Lho, Tae-Jung
    • Journal of the Korea Academia-Industrial cooperation Society
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    • v.9 no.1
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    • pp.1-8
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    • 2008
  • We propose how to program the off-line buffing robot path along shoes' outsole shape in the footwear buffing process by a 5-axis microscribe system like robot mechanism. The microscribe system we developed consists of a 5-axis robot link with a turn table, a signal processing unit, PC and an application software program. Itmakes a robot path on the shoes' upper in accordance with the movement of a microscribe with many joints. The developed system calculates the encoder pulse values for the microscribe arm's rotation and transmits the angle pulse values to the PC through a processing unit. Denavit-Hartenberg's(D-H) direct kinematics is used to make the global coordinate from microscribe joint one. Problems with the microscribe's kinematics can be solved efficiently and systematically by D-H representation. With the coordinate values calculated by D-H equation, our system can draw a buffing gauge-line on the upper sole. We obtain shoes' outline points, which are 2 outlines coupled with the points and the normal vector based on the points. By applying the system to the buffing robot in a flexible manufacturing system, it can be used effectively to program the path of a real buffing robot.

Development of a new Robot Manipulator for shoes Buffing Operation (새로운 신발버핑 작업용 로봇 매니퓰레이터 개발)

  • Hwang, Gyu-Deuk;Oh, Whan-Ju;Choi, Hyeung-Sik
    • Proceedings of the KSME Conference
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    • 2004.11a
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    • pp.743-748
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    • 2004
  • In this paper, an analysis on a new robot manipulator developed for the side buffing of the shoes is presented. The robot is composed of five D.O.F. An Analysis on the forward and inverse kinematics was performed. The hardware system including electric wirings, control system, and related system was developed. Also, The teleoperating communication system was developed to shake with other related system Computer programs to track the bonding line of shoes were developed. An user-friendly graphic program was developed using C $^{++}$ language for the users.

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The Study on the Improvement in Tread Buffing Processing for Recapped Tire for prevention of muscle and skeletal system trouble (근골격계 질환 예방을 위한 재생타이어 트레드 버핑작업 개선에 관한 연구)

  • 김재열;한재호;이연신;김항우;오성민;송경석
    • Proceedings of the Korean Society of Machine Tool Engineers Conference
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    • 2004.04a
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    • pp.197-202
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    • 2004
  • As a part of environmental pollution prevention and resources recycling, the regeneration of waste tire has been largely contributed to national industry. But, the worker has been evaded this regeneration process by reason of the best mischievous process condition among 3D industries. So, the first, the process condition of regenerating waste tire was analyzed. The second, the equipment or system was developed for the improvement of working strength and environment. The last, researchers intend to solve these problems

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Development of Tread Buffing Machine for Recapped Tire for prevention of Musculoskeletal System disorder (근골격계 질환 예방을 위한 재생타이어 트레드 버핑머신 개발)

  • 김재열;한재호;이연신;김항우;오성민
    • Proceedings of the Korean Society of Machine Tool Engineers Conference
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    • 2004.10a
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    • pp.175-180
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    • 2004
  • As a part of environmental pollution prevention and resources recycling, the regeneration of waste tire has been largely contributed to national industry. But, the worker has been evaded this regeneration process by reason of the best mischievous process condition among 3D industries. So, the first, the process condition of regenerating waste tire was analyzed. The second, the equipment or system was developed for the improvement of working strength and environment. The last, researchers intend to solve these problems

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Development of a New Buffing Robot Manipulator for Shoes (새로운 신발 버핑로봇 매니퓰레이터 개발)

  • Hwang Gyu-Deuk;Cho Sung-Duk;Choi Hyeung-Sik
    • Journal of the Korean Society for Precision Engineering
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    • v.23 no.7 s.184
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    • pp.76-83
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    • 2006
  • In this paper, an analysis on a new robot manipulator developed for the side buffing of the shoes is presented. The robot manipulator is composed of five degrees of freedom. An analysis on the forward and inverse kinematics was performed. Through the analysis, an analytic solution was derived for the joint angles corresponding to the position and orientation of the tool in the Cartesian coordinates. The hardware system of the robot composed of the control system, input/output interface system, and related electronic system was developed. The communication system was also developed to interact the robot with the related surrounding systems. A graphic user interface(GUI) program including the forward/inverse kinematics, control algorithm, and communication program was developed using visual C++ language.

A Study on the characteristics of ultra precision about Buffing and Electropolishing for Semiconductor Large Radius Pipe (반도체용 대구경관의 전해 복합연마에 대한 초정밀 가공 특성연구)

  • 이정훈;이은상
    • Proceedings of the Korean Society of Precision Engineering Conference
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    • 2004.10a
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    • pp.609-613
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    • 2004
  • On this study, electrochemical polishing is adapted to ultra-fine surface for semiconductor large radius gas-tube. The system which buffing and electrochemical polishing can be performed simultaneously was constructed in connection with developing exclusive system. Based on existing papers and the research of background, electrode gap and electrolyte flow were fixed. Current density and electrochemical precision time were chosen as variables. On this study, it is objected to find optimal precision condition and precision variables on the in-process electrochemical polishing.

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Effect of Pad Buffing process on Material Removal Characteristics in Silicon Chemical Mechanical Polishing (실리콘 연마에서 패드 버핑 공정이 연마특성에 미치는 영향)

  • Park, Ki-Hyun;Jeong, Hae-Do;Park, Jae-Hong;Kinoshita, Masaharu
    • Journal of the Korean Institute of Electrical and Electronic Material Engineers
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    • v.20 no.4
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    • pp.303-307
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    • 2007
  • This paper investigated the effect of the pad buffing process on the material removal characteristics and pad stabilization during silicon chemical mechanical polishing. The pads surface were controlled by the buffing process using a buffer made by the sandpaper. The buffing process is based on abrasive machining by using a high speed sandpaper. The controlled pad by the buffing process show less deformation deviation and stable material removal rate during the CMP process. In addition, the controlled pad ensure better uniformity of removal rate than comparative pads. As a result of monitoring, the controlled pad by the buffing process demonstrated constant and stable friction force signals from initial polishing stage. Therefore, the tufting process could control the pad surface to be uniform and improve the performance of the polishing pad.

A Study on Adhesion Characteristics for Rubber Parts of Footwear Containing Plasma Treatment (플라즈마 처리에 의한 신발용 고무부품의 접착특성 연구)

  • Jeong, Booyoung;Cheon, Jungmi;Lee, Sangjin;Moon, Jinbok;Chun, Jaehwan
    • Journal of Adhesion and Interface
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    • v.14 no.3
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    • pp.111-116
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    • 2013
  • In this study, we studied surface and adhesion properties with plasma treatment for substitution of buffing and solvent-cleaning in footwear adhesion process. The distance between nozzle and rubber parts was decreased with decreasing the contact angle. And when a speed of plasma treatment increased, the contact angle increased. The result of surface roughness, Ra and Rz increased in 20% and 16% after the plasma treatment. The distance of between nozzle and rubber parts was decreased with decreasing the peel strength. And the speed of plasma treatment was increased with decreasing the peel strength.

A Study on Adhesion of Mechanical Properties of Rubber by MgCl2 (MgCl2에 의한 고무의 접착특성 및 기계적 강도 변화)

  • Kim, Seong-Hye;Jeon, Jun-Ha;Um, Gi-Yong
    • Journal of Adhesion and Interface
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    • v.18 no.2
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    • pp.53-58
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    • 2017
  • In this study, to overcome a complicated shoe adhesion process such as buffing, pre-treatment by primer in the rubber component of the shoe, we studied adhesion and mechanical properties with rubber compound added $MgCl_2$. We determined adhesion properties of $MgCl_2$ content. Especially, the rubber containing $MgCl_2$ exhibited good adhesion properties to water-based adhesion. Since $MgCl_2$ is a water-soluble salt, it was judged that this phenomenon occurred. The results are confirmed by contact angle and surface morphology measurement. In addition, in the case of rubber compound added $MgCl_2$, the crosslinking efficiency was increased and the NBS resistance was increased.

A Study on Adhesion of Mechanical Properties of Rubber by Water-soluble salt (수용성염에 의한 고무의 접착특성 및 기계적 강도)

  • Kim, Seong-hye;Jeon, Jun-Ha;Um, Gi-Yong
    • Journal of Adhesion and Interface
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    • v.19 no.2
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    • pp.55-59
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    • 2018
  • In this study, to overcome a complicated shoe adhesion process such as buffing, pre-treatment by primer in the rubber component of the shoe, we studied adhesion mechanical properties with rubber compound added water-soluble salt for the purpose of improving the adhesion between midsole and outsole. Acid salts, basic salt and neutral salts were evaluated, rubber containing basic salts showed excellent adhesion to water-based adhesion. Since the basic salt is present as the hydroxy salt, the surface of rubber is hydrophilized. The results are confirmed by contact angle and IR spectroscopy measurement. In addition, in the case of rubber compound added basic salts, NBS abrasion resistance and hardness were increased by increasing crosslink density, but crosslink time was delayed.