• Title/Summary/Keyword: 단일 화학종 비반응모델

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A Computational Study on Cooling Analysis of the Flame Deflector for the 75 tonf Class Propulsion Test Facility (75톤급 추진기관 시험설비 화염유도로 냉각해석에 관한 수치적 연구)

  • Moon, Seong-Mok;Cho, Nam-Kyung;Kim, Seong-Lyong;Jun, Sung-Bok;Lee, Kyoung-Hoon;Kim, Dong-Hwan
    • Journal of the Korean Society of Propulsion Engineers
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    • v.19 no.2
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    • pp.55-64
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    • 2015
  • In this study, a 3-D flame cooling analysis is conducted to examine thermal safety for the flame deflector of the 75 tonf class propulsion test facility, and the safe discharge of the exhaust gas is assessed by using numerical results. The Mixture multiphase model is adopted for the simulation of heat transfer and phase exchange process between flame and cooling water, and the computational study using the single species unreacted model for the exhaust plume is carried out for the flame cooling. Numerical analysis predicts maximum temperature on the flame deflector wall for different water flow rates, and evaluates the safe minimum flow rate of water corresponding to the fire-resistant temperature for concrete.

Preliminary CFD Results of a Dual Bell Nozzle based on the KSLV-II (한국형발사체를 기반으로 한 듀얼 벨 노즐의 전산수치해석 기초 결과)

  • Kim, Jeonghoon;Choi, Junsub;Huh, Hwanil
    • Journal of the Korean Society of Propulsion Engineers
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    • v.20 no.6
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    • pp.18-28
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    • 2016
  • Numerical analysis was conducted as a preliminary study for evaluating the dual bell nozzle. For future parametric studies, a dual bell nozzle was designed, and thereafter inlet condition, turbulence model, and the number of optimum grids were determined. Dual bell nozzle was designed based on the KSLV-II first stage nozzle. Inlet condition was determined to frozen flow model of non-reacting eight species by comparing with the design values. SST $k-{\omega}$ model turned out to be suitable as turbulence model. About 150 thousand of the grids were selected after grid sensitivity tests. Based on the results determined in this study, we plan to investigate performance gain of the KSLV-II by adopting a proposed dual bell nozzle.