Enhancement of Desulfurization System Efficiency in 1,000 MW Coal-Fired Power Plants

1,000 MW 석탄화력발전소 대기환경오염물질 제거효율 향상을 위한 탈황설비 성능개선

  • Lee, Young-Su (Department of Power Engineering, Hanyang University) ;
  • Moon, Seung-Jae (Department of Mechanical Engineering, Hanyang University)
  • 이영수 (한양대학교 파워엔지니어링공학과) ;
  • 문승재 (한양대학교 기계공학부)
  • Received : 2020.08.30
  • Published : 2021.06.30

Abstract

Recently, air environmental issues such as fine dust have rapidly emerged as national issues, and intensive environmental regulations are being applied to coal-fired power plants. This study introduces the case of improving the performance of desulfurization facilities for removing sulfur oxides and dust, which are the main air pollutant emitters of coal-fired power plants, and conducted four case studies to improve the performance of 1,000 MW power plants currently in operation and carried out construction. Liquid ratio was increased by remodeling the absorption tower of desulfurization facilities, and vaporization reaction was promoted by increasing the flow rate of oxidized air. In addition, the gas heater leakage rate was improved to improve the efficiency of final desulfurization facilities. It is expected that performance improvement work considering harmony with existing facilities will satisfy the regulations(25ppm of sulfur oxides, 5mg/Sm3) that will be applied from 2023, and can be referred to other thermal power plants for review and application.

최근 미세먼지 등 대기환경 문제가 국가적 이슈로 급부상 하고있는 추세이며 특히 석탄화력발전소에 대한 강도높은 환경규제치가 적용되고 있는 실정이다. 본 연구는 석탄화력발전소 주요 대기오염 배출물질인 황산화물과 먼지 제거를 위한 탈황설비 성능개선 사례에 대해 소개하고 있으며 현재 운영중인 1,000 MW 발전소의 성능개선을 위한 네가지 Case Study를 수행하고 공사를 하였다. 탈황설비 흡수탑 개조를 통해 액기비를 증대시켰으며 산화공기 유량을 증대시켜 기액 반응을 촉진하였다. 또한 가스가스히터 누설률을 개선하여 최종 탈황설비 효율을 향상시켰다. 기존 설비와 조화를 고려한 성능개선 공사를 통해 2023년부터 적용될 규제치(황산화물 25ppm, 먼지 5mg/Sm3)를 만족할 것으로 예상되며 타 화력발전소에 검토 및 적용하는데 참고될 수 있다고 기대된다.

Keywords

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