500 MW 석탄화력발전소 촉매단추가에 따른 탈질설비 효율에 미치는 영향

Effect of addition of a catalystic layer on Denitrification System efficiency in a 500 MW Coal-fired Power Plant

  • 이상수 (한양대학교 파워엔지니어링공학과) ;
  • 문승재 (한양대학교 기계공학부)
  • Lee, Sang Soo (Department of Power Engineering, Hanyang University) ;
  • Moon, Seung-Jae (Department of Mechanical Engineering, Hanyang University)
  • 투고 : 2020.08.30
  • 발행 : 2021.03.31

초록

최근 미세먼지 등 대기오염물질 배출에 대한 전국민적 우려로 정부는 대기오염물질 배출규제 강화정책을 내놓고 있다. 국내 석탄화력발전소는 대기환경설비 성능개선에 박차를 가하고 있으며, 이 논문에는 500 MW급 표준석탄화력 탈질설비에 촉매단을 추가하는 성능개선사례를 다루고 있으며, 촉매단 추가 전·후 성능시험시험과 NOx제거효율에 따른 탈질설비 핵심성능 인자의 변화를 살펴보았다. 연구결과 촉매단 추가 전·후 탈질설비 효율은 80%에서 88%로 상승했고, 핵심성능인자인 미반응 암모니아, SO2/SO3 전환율은 설계보증치를 만족하였으나, 차압의 경우 설계보증치를 초과하였다. 동시에, NOx 제거효율에 따른 핵심성능인자 변화는, 미반응 암모니아 농도, 차압 항목은 NOx 제거효율이 증가에 따라 같이 증가하는 양상을 보여 관리 및 개선이 필요하다는 결과를 얻을 수 있었다.

The government has recently come up with a policy to tighten regulations on air pollutant emissions due to public concerns over the emission of pollutants such as fine dust. The coal-fired power plant is speeding up the improvement of the performance of environmental facilities, and this paper deals with the cases of performance improvement by adding a catalyst to the 500 MW standard coal-fired power DeNox system, and examines the change in the performance factors according to the addition of catalysts and the efficiency of NOx removal. The DeNOx efficiency before and after improvement increased from 80% to 88%, and the conversion rate of SO2/SO3, ammonia slip which are performance factors satisfied the design assurance value, but exceeded the design assurance value for differential pressure. At the same time, the ammonia slip concentration and differential pressure items increased as the NOx removal efficiency increased, resulting in the need for management and improvement.

키워드

참고문헌

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