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아레나 시뮬레이션을 활용한 화장품 포장공정의 개선사례 연구

A Study on the Improvement Case of Cosmetic Packaging Process Using ARENA Simulation

  • 이남수 (한밭대학교 스마트생산경영공학과) ;
  • 이재용 (한밭대학교 스마트생산경영공학과) ;
  • 조은현 (한밭대학교 스마트생산경영공학과) ;
  • 이동형 (한밭대학교 스마트생산경영공학과)
  • Lee, Nam-Su (Dept. of Smart Production & Management Engineering, Hanbat National University) ;
  • Lee, Jae-Yong (Dept. of Smart Production & Management Engineering, Hanbat National University) ;
  • Jo, Eun-Hyeon (Dept. of Smart Production & Management Engineering, Hanbat National University) ;
  • Lee, Dong-Hyung (Dept. of Smart Production & Management Engineering, Hanbat National University)
  • 투고 : 2020.04.29
  • 심사 : 2020.06.25
  • 발행 : 2020.06.30

초록

Demand for cosmetics with functionality and eco-friendliness has increased dramatically due to recent aging, well-being trends, and increased interest in beauty. Cosmetics production in 2014 was 8,970.4 billion won, an increase of about 50% compared to 6,014.6 billion won in 2010. In the midst of this, similar companies in intense competition are pursuing differentiated strategies and innovation activities to solve quality, price and delivery problems. In particular, cosmetics packaging work is getting more difficult due to the increasing bill of materials (BOM) and difficult assembly methods. Therefore, in this study, the following problems were identified and suggestions for the improvement of the packaging Many research laboratories such as biotechnology, chemistry, and pharmaceuticals, which are undergoing various studies, are equipped with ready-made laboratory safety equipments such as bio-safety workbenches, aseptic bases, and exhaust workbenches. However, most researchers are disadvantaged in using existing safety equipment. This is because existing safety equipment can not take into account all of the unique characteristics of the research. For this reason, researchers are demanding the development of customized safety equipment that is well suited to their research needs. process of Company C, which is facing difficult situation to respond to the customer 's delivery due to the 52 - hour work week. First, we used the stopwatch to find the difficulty process in the packaging process and show ways to improve it. Second, to improve the efficiency of line balancing in the packaging process, we integrate processes, improve work methods, and perform simple automation. As a result, the prepare loss for replacement was reduced by 1 minute from 5 minutes, resulting in a 23% increase in productivity from 112 ea./hour to 137ea./ hour per person. At this time, the LOB of the packaging process was improved from 70% to 82% by operating one more production line through one person per line, total 9 people saving.

키워드

참고문헌

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