입상활성탄 흡착지 운영에서 역세척 주기와 팽창률의 영향 평가

Decision of Backwashing frequency and method on the GAC adsorber

  • 채선하 (한국수자원공사 K-water연구원) ;
  • 조창현 (한국수자원공사 고양권관리단) ;
  • 이희대 (한국수자원공사 감사실) ;
  • 왕창근 (충남대학교 환경공학과)
  • 투고 : 2010.10.11
  • 심사 : 2010.12.14
  • 발행 : 2010.12.15

초록

The objective of this study was to evaluate the backwashing frequency and method on the Granular Activated Carbon (GAC) in G WTP. A backwashing period was determined as 50 days and 60 days, respectively. Prior to Backwashing by head loss build, biomass concentration in effluent as constant and DO concentration was maintained more than 11.5 mg/L in GAC bed. Peak turbidity of backwashing water was 73.6~303 NTU. Mean turbidity of backwashing water at initial 9 minute of backwash operation was 50.7~82.8 NTU. After 30 minute backwashing operation, final turbidity reaches approximately 10 NTU. The frequency of backwashing and turbidity of backwashing water overtime were evaluated. At 20days of backwashing frequency, the peak turbidity was 73 NTU and 42 NTU respectively when 10% and 25% of expansion of GAC were applied. At 14 minute of backwashing time, it was observed that turbidity of 10% expansion of GAC was higher than that of 20% expansion.

키워드

참고문헌

  1. Bouwer, E. J. and Crowe, P. B. (1988) Biological processe s in drinking water treatment, J. of AWWA, 90(1), pp. 71-85.
  2. Amirtharajah, A. (1991) Optimum backwash of dual media filter and GAC filter adsorbers with air scour, AWWAHF.
  3. Rice, R. and Robson, M. (1982) Biological Activated Carbon Enhanced Aerobic Biological Activity in GAC System, Ann Arbor Science Publ., Ann Arbor, MI. USA.