The decision of the inner fault of 154kV Gas Insulated Transformer through analyzing ingredients of insulated gas.

절연가스 성분분석을 통한 154kV 가스절연변압기 내부결함 판정

  • Mun, Byong-Seon (Seoul Head Quarters of Korea Electric Power Corporation) ;
  • Tark, Eui-Gyun (Seoul Head Quarters of Korea Electric Power Corporation) ;
  • Lee, Tae-Kyu (Seoul Head Quarters of Korea Electric Power Corporation) ;
  • Park, Chan-Eui (Seoul Head Quarters of Korea Electric Power Corporation) ;
  • Lee, Min-Ho (Seoul Head Quarters of Korea Electric Power Corporation)
  • 문병선 (한국전력공사, 서울지역본부) ;
  • 탁의균 (한국전력공사, 서울지역본부) ;
  • 이태규 (한국전력공사, 서울지역본부) ;
  • 박찬의 (한국전력공사, 서울지역본부) ;
  • 이민호 (한국전력공사, 서울지역본부)
  • Published : 2015.07.15

Abstract

In order to looking for method of detecting inner fault of a 154kV GIT(Gas Insulated Transformer), it was considered that diagnosis partial discharge(PD) in UHF band and that analyze the ingredients of SF6 insulating gas. UHF PD diagnosis that is optimized to GIS was considered unsuitable through checking of inner part of a transformers which PD is detected excessively. The method analyzing the content of six kinds of gas(SOF2, SO2F2, etc)was decided through analysis of chemical degradation and combination process and discharge experiment. With the result applying this method to analyze the content of insulated gas of eighty five Gas Insulated Transformers.

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