A Case Study for Deformation of Caisson caused by Friction Shortage

케이슨 하부의 마찰저항 부족에 따른 케이슨 안벽 변위발생 사례연구

  • 심동현 (현대건설 기술개발원 설계실) ;
  • 박준호 (현대건설 기술개발원 설계실) ;
  • 이경숙 (현대건설 기술개발원 설계실)
  • Published : 2008.10.10

Abstract

Deformation of caisson occurred during the backfilling behind the caisson and some caisson moved toward seaside. A series of site investigation were conducted to figure out various circumstances at site and also used to analyze the cause of deformation. The soil condition of backfilling is also investigated because dredged material was used as a backfill material. The friction angle of backfill is supposed to be lower than the estimated one which was used in design stage. To determine the cause of friction shortage, back analysis for sliding safety were carried out with considering the soil condition of backfilling. A remedial plan, re-rising and relocating a caisson with backfilling good earth after treatment of caisson rubble mound to achieve the safety for sliding was proposed as a best solution based on the back analysis results. Reform concrete structure including service gallery and crane rail was also considered with the remedial work to improve the cape line of caisson.

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