Proceedings of the KSR Conference (한국철도학회:학술대회논문집)
- 2006.11b
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- Pages.1364-1368
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- 2006
A Reinforcement Effect of Pile Foundation by Compaction Grouting System in Railroad Station Building
Compaction Grouting System에 의한 철도역사건물 파일기초보강효과
- Published : 2006.11.09
Abstract
By the countermeasure which is caused by with railroad station ground settlement it applied a CGS in each independent foundation. The effectiveness of the ground improvement and the bearing capacity of the compaction pile has been verified by the Cone Penetration Test(CPT) and Load Test. Test result show that penetration resistance and the cone friction force increased a lot and settlement 13.475mm as the standard settlement 40.0mm appeared at below. Also uniaxial compression test result
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