RBM 굴착에 따른 수직구의 3차원적 거동 연구

A study on the 3-dimensional behavior of shaft by the RBM reaming

  • 조만섭 ((주)유니벡 토목사업2본부) ;
  • 이석원 (한국건설기술연구원 토목연구부) ;
  • 마상준 (한국건설기술연구원 토목연구부)
  • 발행 : 2002.03.01

초록

To investigate the behavior of air-shaft and existing tunnel by excavating the small-diameter shaft into the existing tunnel, prototype air-shaft was constructed and analyzed in this study. Geotechnical characterization was conducted by boring and rock cores obtained were tested in the laboratory. Field monitoring including radial and tangential stresses and displacements was conducted with the 3-dimensional numerical analysis of prototype air-shaft. Results of field monitoring were compared with the numerical results. The results showed that maximum displacement of 2.11mm and maximum tangential stress of 54.0 kg/$\textrm{cm}^2$ were obtained during shaft excavation near the right shoulder of the existing tunnel. The comparison of these field measurements with 3-dimensional numerical analysis showed that much more higher stress was measured during excavation compared to the numerical results even though the trends of stress and displacement were similar.

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