Case Study on Seepage Analysis and Countermeasure Against the Seepage Flow of In-ground LNG Storage Tank

LNG 지하저장탱크의 침투해석 및 용수 대책공법에 대한 사례분석

  • 신은철 (인천대학교 토목환경시스템공학과) ;
  • 오영인 (인천대학교 대학원 토목환경시스템공학과) ;
  • 이상혁 (인천대학교 대학원 토목환경시스템공학과)
  • Published : 2001.03.01

Abstract

Since Pyoungtaek thermal power plant began using natural gas in 1986, the annual using volume has rapidly increased and reached 12.7 million tons in 1999. When the natural gas is cooled to a temperature of approximately -162$^{\circ}$C at atmospheric pressure, it condenses to a liquid called liquefied natural gas(LNG). LNG has a special characters such as odorless, colorless, non-corrosive, and non-toxic. So, LNG storage tank, tanker ship, transfer pipelines are required the special storage and transportation systems and technology. The presently operating LNG terminals are Pyongtaek and Inchon terminals. A total of 19 above-ground LNG storage tanks(100 thousand ㎘ grade) are currently in operation with a sendout capacity of 4,360tons/hour. To meet the growing domestic demand of LNG supply, the Inchon receiving terminal is expanding(six in-ground tank) and constructing a third LNG terminal at Tongyong. In this paper, case study on seepage analysis and countermeasure against increasing the seepage volume of in-ground LNG storage tank excavation work is reported. The results of an additional seepage analysis are presented to verify the design seepage volume of assumption section and seepage volume after curtain-grouting in the slurry wall.

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